BACKGROUND OF THE INVENTION
[0001] According to modem quantum theory, the chemical and physical properties of substances
arise fundamentally from electrodynamic interactions. Modifying these interactions
can alter electronic structures and thereby endow the elements of the periodic table
and their compounds with new properties.
[0002] United States Patent No.
6,572,792, which is incorporated herein by reference, to Christopher J. Nagel describes a process
for modifying the electronic structure of a material and of the products that are
produced by the process. For example, this patent describes metals, such as copper,
cobalt, nickel, and alloys thereof, that possess novel properties, such as novel XRF
patterns and magnetic properties. However, it is desired to further amplify or modify
the effects achieved by the process.
SUMMARY OF THE INVENTION
[0003] The present invention relates to improved methods of modifying the electronic structure
of a material. The process includes the iterative and/or cyclic addition of energy
to a material.
[0004] In one embodiment, the present invention includes a method of processing a metal
or an alloy of metals, comprising the steps of:
- (1.) Melting the material;
- (2.) Adding a carbon source to the material; and
- (3.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein the material remains at a temperature above the melting point
during the entire step.
[0005] The process can further comprise one or more of the steps, in one or more iterations
or cycles:
(4.) Adding a flow of a gas (such as nitrogen, hydrogen and/or a noble gas) through
the material;
(5.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein the material remains at a temperature above the melting point
during the entire step;
(6.) Adding a carbon source to the material; and/or
(7.) Holding the material with optional gas addition.
[0006] The process in a preferred embodiment involves one or more iterations or cycles of
adding energy to a material in a supersaturated state with carbon. In this embodiment,
the process comprises, or further comprises, one or more of the steps, in one or more
iterations or cycles:
(8.) Lowering the temperature of a molten material, wherein the material becomes supersaturated
with carbon;
(9.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein supersaturation with carbon is maintained and the material remains
at a temperature above the melting point during the entire step, optionally in the
presence of gas addition during the entire step or any portion of the step (e.g.,
during one or more or all of the steps wherein temperature increases or decreases);
(10.) Holding the material at a selected temperature, optionally in the presence of
gas addition;
(11.) Cooling the material, such that the material continues to be supersaturated
with carbon and the material remains at a temperature above the melting point, optionally
in the presence of gas addition; and/or
(12.) Cooling the material to room temperature, thereby obtaining a solidified manufactured
material.
[0007] In one embodiment, steps 8 and 9 (or 9 and 11) are performed and repeated 1, 2, 3,
4 or more times, preferably 4 or more times.
[0008] In preferred embodiments, the improvement in the processes of the invention comprises
at least one of the following:
- (a) the gas or gaseous addition (e.g., nitrogen, hydrogen, and/or noble gas) is added
to the material through a lance set at a level above the liquid level;
- (b) at least one of the gases or gaseous additions comprises a gas mixture;
- (c) at least one of the gases has been exposed to radiation;
- (d) current, e.g., AC or DC current, is added to the material in a further step or
during one or more of the above steps;
- (e) during the cooling step, a gas is added to the material; and/or
- (f) during the cooling step, the material is quenched with water wherein the water
is not stirred;
- (g) at least one form of radiation has been filtered;
- (h) the material is exposed to radiation in a further step or during one or more of
the above steps; and/or
- (i) varying the reactor power (e.g., above normal holding power) between two power
levels over ½, one or more cycles.
[0009] Advantages of the present invention include a method of processing metals into new
compositions of matter and producing and characterizing compositions of matter with
altered physical and/or electrical properties.
DETAILED DESCRIPTION OF THE INVENTION
[0010] United States Patent No.
6,572,792 to Christopher J. Nagel describes a process for modifying the electronic structure of a material and to the
products that are produced by the process. For example, this patent, which is incorporated
herein by reference in its entirety, describes metals, such as copper, cobalt, nickel,
and alloys thereof, that are induced by the process to acquire novel properties, such
as novel XRF patterns and magnetic properties. As described in that patent, electromagnetic
chemistry is the science that affects the transfer and circulation of energy in many
forms when induced by changes in electromagnetic energy. In empty space, a constant
speed for light, independent of the frame of reference (i.e., "each ray of light moves
in the coordinate system 'at rest' with the definite velocity V independent of whether
this ray of light is emitted by a body at rest or a body in [uniform] motion") as
advanced in "The Theory of Electrodynamics of Moving Bodies" (Einstein, 1905) implicitly
embeds a discrete partition between its associated coordinate system at rest and the
reference systems that are relative to it. A topological description of this partition,
satisfying the postulates advanced in the above referenced paper, requires that when
the electrodynamic components of matter are manipulated, discrete changes in energy
exchange occur between meromorphic constructions while continuous changes in energy
exchange occur along holomorphic mappings. Harmonics governing the redistribution
of energy are the vehicles by which changes in (material) properties, such as the
magnitude and/or the orientation, can occur. Alignment of the electrodynamic component
induces effects that may result in significant changes in the underlying material
species: (1) alignment of atoms with the resulting directionality of physical properties;
(2) alignment of energy levels and the capability to modify harmonic structure, may
establish physical properties conducive for energy transfer; (3) alignment of the
electrodynamic component includes the opening of pathways for free electron flow,
and; (4) alignment of electrodynamic field phase orientation.
[0011] The present invention relates to new materials and compositions of matter, and includes
manufactured, or tailored, metals or alloys of metals. A "manufactured" or "tailored"
metal or alloy is a metal or alloy, which exhibits a change in electronic structure,
such as that seen in a fluid or adjustable XRF spectrum.
The American Heritage College Dictionary, Third Edition defines "fluid" as changing or tending to change.
[0012] Metals of the present invention are generally p, d, or f block metals. Metals include
transition metals such as Group 3 metals (e.g., scandium, yttrium, lanthanum), Group
4 metals (e.g., titanium, zirconium, hafnium), Group 5 metals (vanadium, niobium,
tantalum), Group 6 metals (e.g., chromium, molybdenum, tungsten), Group 7 metals (e.g.,
manganese, technetium, rhenium), Group 8 metals (e.g., iron, ruthenium, osmium), Group
9 metals (e.g., cobalt, rhodium, iridium), Group 10 metals (nickel, palladium, platinum),
Group 11 metals (e.g., copper, silver, gold), and Group 12 metals (e.g., zinc, cadmium,
mercury). Metals of the present invention also include alkali metals (e.g., lithium,
sodium, potassium, rubidium, and cesium) and alkaline earth metals (e.g., beryllium,
magnesium, calcium, strontium, barium). Additional metals include aluminum, gallium,
indium, tin, lead, boron, germanium, arsenic, antimony, tellurium, bismuth, thallium,
polonium, astatine, and silicon.
[0013] The present invention also includes alloys of metals. Alloys are typically mixtures
of metals. Alloys of the present invention can be formed, for example, by melting
together two or more of the metals listed above. Preferred alloys include those comprised
of copper, gold, and silver; tin, zinc, and lead; tin, sodium, magnesium, and potassium;
iron, vanadium, chromium, and manganese; nickel, tantalum, hafnium, and tungsten;
copper and ruthenium; nickel and ruthenium; cobalt and ruthenium; cobalt, vanadium
and ruthenium; and nickel, vanadium and ruthenium.
[0014] The material can be added, or charged, to the reactor in a variety of forms. For
example, where the material is a metal, it can be convenient to add the material as
powder, flakes, pellets or ingots. The material can be charged all at once or in stages,
including continuously during the initial melt or energy addition step.
[0015] The backspace of the reactor can be advantageously purged by a gas, such as a gas,
as described below, or other gas. Nitrogen is a convenient gas for this purpose. In
one example, a nitrogen flow is maintained throughout an entire method, such that
a nitrogen pressure of about 0.4-0.6 psig or about 0.5 psig is maintained. Alternatively,
other gases, such as argon may be used for such purposes.
[0016] Carbon sources of the present invention include materials that are partially, primarily,
or totally comprised of carbon. Suitable carbon sources include graphite rods, graphite
powder, graphite flakes, fullerenes, amorphous carbon, diamonds, natural gas, methane,
ethane, propane, butane, pentane, and combinations thereof. A preferred carbon source
has a high purity (<50 ppm, such as <10 ppm, preferably <5 ppm impurities). The carbon
source is selected, in part, based on the system to which it is added. In one example,
graphite rods and graphite flakes are added in a sequential manner. In another example,
the carbon source can be added as a gas, such as through the introduction of methane.
[0017] Carbon sources can be contacted with the material for variable periods of time. The
period of time the carbon source is in contact with the material is the time between
adding the carbon source and removing the undissolved carbon source. The period of
time can be from about 0.5 hours to about 12 hours, about 1 hour to about 10 hours,
about 2 hours to about 8 hours, about 3 hours to about 6 hours, about 3.5 hours to
about 4.5 hours, or about 3.9 hours to about 4.1 hours. Alternatively, the period
of time can be from about 5 minutes to about 300 minutes, about 10 minutes to about
200 minutes, about 20 minutes to about 120 minutes, about 30 minutes to about 90 minutes,
about 40 minutes to about 80 minutes, about 50 minutes to about 70 minutes, or about
59 minutes to about 61 minutes. As can be seen above, the process of the invention
relies in part upon the cyclic, iterative and/or harmonic addition of energy to the
material. In general, the carbon contact period will coincide with a cycle, series
of cycles or iteration of steps.
[0018] A cycle of the present invention includes a period of time where the energy of a
material is varied between a first and second selected energy endpoints with a return
to the first energy endpoint. A half cycle is the completion of a single sweep or
variant between a first and second energy endpoint. A full cycle is the completion
of two sweeps between the first and second energy endpoints. A cyclic step refers
to the repetition of two or more cycles without substantially changing the endpoints
of each sweep. Iterations generally refer to the repeating of two or more steps, such
as a cyclic step in combination with a cooling step.
[0019] An energy level, such as an endpoint, can often be conveniently measured by the material's
(e.g., metal's) temperature and/or the degree to which a material (e.g., metal) is
saturated with a second component (e.g. carbon). Over a period of time, varying the
temperature involves a period of raising (or increasing) the temperature of a material
(e.g., metal or alloy) and a period when the temperature of a material (e.g., metal
or alloy) decreases (either passively, such as by convection or heat transfer to the
surrounding environment, or actively, such as by a mechanical means or cooling, e.g.,
quenching). The time period of each sweep can be selected to produce a harmonic energy
pattern. The time period is also, in part, dictated by the rate of heating and cooling
which is practical by the equipment (e.g., induction furnace) used, the material selected
and the mass of material being processed. In some experiments, a cycle comprising
a 7 minute period to increase the energy level (sweep up) and a 7 minute period to
decrease the energy level (sweep down) was used. However, other time periods (e.g.,
2, 3, 4, 5, 6, 8, 9, 10, 20 or more minutes) can be used. Further, combinations can
be used (7 minutes up and 5 minutes down). Where energy is added to a material by
other means (e.g., ultraviolet or infrared radiation, current or reactor power), the
time periods are not limited by the rate of heating or cooling the material.
[0020] Increasing the temperature of the metal or alloy increases the amount of carbon that
can be dissolved into that metal or alloy, which therefore decreases the degree to
which the metal or alloy is saturated with carbon (relative to the temperature and
degree of carbon saturation when graphite saturation assemblies are removed the first
time). Similarly, decreasing the temperature of the metal or alloy increases the (relative)
degree to which the metal or alloy is saturated with carbon. Thus, carbon saturation
levels of a material can also be used to measure or determine energy endpoints. Where
the material to be modified is a non-metal (e.g., carbon, gas), the energy endpoints
are better measured by temperature or associated emission spectra.
[0021] A cycle can also include, or be interrupted or ended with, a holding step. Thus,
the material can be held at an energy level (as measured, for example, by the temperature
or degree of carbon saturation) for a selected period of time. The holding period
can be several minutes to several hours or more. In one example, the material was
held for 60 minutes. In another example, the material was held for 5 minutes. More
than one hold step can be incorporated into the process and can be included in an
iteration of steps.
[0022] The degree to which a metal is saturated with carbon varies over the course of the
process, as well as within a step. For example, the degree of carbon saturation can
vary between 70% and 95% in the first cycling step, between 80% and 95% in the second
cycling step, between 101% and 103% in the third cycling step, between 104% and 107%
in the fourth cycling step, between 108% and 118% in the fifth cycling step, and between
114% and 118% in the sixth cycling step. It is preferred to conduct 4 or more supersaturation
steps. Supersaturation is defined herein as follows:
+n%wt represents the weight percent above the equilibrium saturation value of the material
in its natural state. For example, +1%wt represents 1%wt above the saturation value as defined in its natural or naturally occurring state.
[n]eqsat represents the equilibrium saturation of "n" in its natural state. For example, [C]eqsat represents the equilibrium saturation of carbon for the thermodynamic state specified
(e.g., T, P, composition) when the composition is in its natural, or naturally occurring,
state.
[0023] Gas, such as nitrogen, hydrogen or a noble gas, can be added during a cycle, except
where it is specified that gas addition is ceased prior to that cycle. The gas provides
a third body effect for the reaction facilitating energy exchange. For example, hydrogen,
helium, nitrogen, neon, argon, krypton, xenon and carbon monoxide can be added. In
a preferred embodiment, the gas is added as a mixture. A preferred mixture comprises
argon, helium, neon and/or krypton. Preferably, at least 50%, more preferably at least
80% such as at least 90% by volume argon, helium or hydrogen is present in the mixture.
Particularly preferred mixtures, by volume, include (1) 93% argon, 5% helium and 2%
neon; (2) 92% argon, 5% helium and 3% neon; (3) 95% argon and 5% helium or neon; (4)
95% helium and 5% krypton; (5) 95% nitrogen and 5% helium; (6) 97% helium and 3% neon
(optionally trace amounts of krypton); (7) 97% argon and 3% neon; (8) 60% argon and
40% helium (optionally trace amounts of neon, hydrogen and/or krypton); (9) 49.5%
hydrogen, 49.5% helium and 1% neon. In selecting the specific combination and concentrations
of the gases, the following factors should be considered: emission profile, Hodge
spectral character and required momentum/energy exchange.
[0024] In each embodiment, the gas can be added at various rates. In general, the gas is
added in terms of the resulting agitation on the material and exchange with the material.
As such, the gas can be added at a low rate, resulting in low agitation/exchange;
at a modest, moderate or high or vigorous rate. The gases can be mixed prior to adding
or added individually. Using conventional fluid dynamic scaling models and assuming
a crucible size of 3.75 inches I.D., with a 14.5 inch height, holding 20 lbs of cobalt,
examples of low agitation can be achieved by adding about 0.25 SLPM; modest agitation
can be achieved by adding between about 1.25 SLPM; moderate agitation can be achieved
by adding between about 2.5 SLPM and high agitation can be achieved agitation by adding
between about 5.0 SLPM. Selecting low agitation generally results in clearly defined
bubbles in a quiescent bath. High agitation generally results in a turbulent well-mixed
bath. Modest and moderate agitation rates enables mixing and exchange to be adjusted
between these extremes. In some instances, the rate of addition can begin at one level
and be changed during the step to a different level (e.g., from a low rate to a vigorous
rate). In general, it is desirable to add the gas at a rate of excess to assist in
controlling the reaction and ensuring that rate limiting steps are not associated
with mass transfer diffusion. Flow rates for a crucible size of 8.875 inches, with
a 16.5 inch height, holding 100 lbs of copper can be determined using standard scaling
techniques based on bubble size and residence time distributions to achieve similar
transport phenomena.
[0025] The gas can be added to the material either below or above (including across) the
surface level of the material. When the gas is added below the surface level, it can
be added via injection ports from the bottom or sides of the reactor. However, it
is often preferred to add the gas via a lance. The lance can be positioned to provide
gas entry below the surface level, e.g. at the bottom of the reactor, midpoint or
near the surface of the material. When the lance is to be submerged, it is often desirable
to position the lance prior to or during the initial charging of the reactor with
the material (e.g., as the reactor is being packed with metal pellets). Where the
lance is not submerged, the lance can be placed to direct the gas across the surface
of the material or toward at the surface. Where the gas is directed toward the material,
the gas can be directed at a force that creates an indentation in the surface. The
lance can be placed along the centerline of the reactor. However, it is often desirable
to place the lance off center, e.g., at about two thirds radius point as measured
from the center. Lance placement involves consideration of mass/energy transfer, interaction
of multiple lances, and harmonic character of the reactants being added.
[0026] The material can be subjected or exposed to the gas either during the entire process
or a cycle or series of cycles or alternating cycles, during the cooling step or thereafter
as a post treatment step.
[0027] Superior results in controlling the reaction have been achieved by exposing at least
one gas to radiation. The exposure can be applied in a continuous or batch mode. For
example, the radiation source can be applied as the gas moves through a conduit for
the gas source to the reactor. The conduit is preferably not opaque and is more preferably
translucent or transparent. The radiation can be applied in an open or closed system.
A closed system entails exposing the gas to the specified radiation in the substantial
absence of other radiation sources (e.g., visible light, magnetic fields above background).
This can be easily accomplished by building a black box surrounding a segment of the
conduit and placing the radiation source(s) within the black box. An open system can
also be employed where the radiation source(s) are not shielded from ambient light.
[0028] In yet other embodiments, the material itself can be subjected to radiation, either
during or after the processes described herein. For example, a tailored metal can
be subjected to radiation to further modify the properties of the metal.
[0029] The radiation sources can be selected to provide a broad range of emitted wavelengths.
For example, the radiation can range from infrared to ultraviolet wavelengths. In
one embodiment, examples of preferred radiation sources emit into the range of 160
nm to 1000 nm; in another embodiment, examples of preferred radiation sources emit
and into the range of 180 nm to 1100 nm; and in a more preferred embodiment examples
of preferred radiation sources emit into the range of 400 nm to 700 nm. The radiation
can be conveniently supplied by short arc lamps, high intensity discharge lamps, pencil
lamps, lasers, light emitting diodes, incandescent, fluorescent, and/or halogens for
example. Examples of suitable high intensity discharge lamps include mercury vapor,
sodium vapor and/or metal halide. Short arc lamps include mercury, xenon or mercury-xenon
lamps. Pencil lamps include neon, argon, krypton, xenon, short wave ultraviolet, long
wave ultraviolet, mercury, mercury/argon, mercury/neon, and the like. The radiation
can also include (or exclude), incandescent or fluorescent light and/or natural sources
of light, such as electromagnetic radiation emitted by celestial bodies.
[0030] The radiation sources can optionally be used in combination with light shields or
wavelength filters. Examples of suitable shields and filters can be obtained from
UVP, Inc. (Upland, CA). The filters and shields can direct or modify the emission
output. Examples of UVP Pen-Ray Filters include the G-275 filter which absorbs visible
light while transmitting ultraviolet at 254 nm and the G-278 filter which converts
shortwave radiation to longwave radiation at 365 nm. Pen-Ray Shields include Shield
A which has a 0.04 inch ID hole for point-like source, Shield B which has a 0.31 x
0.63 inch window, and Shield C which has a 0.19 x 1.5 inch window. Filters and shields
can also be obtained from Newport Corp. (Irvine, CA). The Newport 6041 Short Wave
Filter absorbs visible lines; the 6042 Long Wave Conversion Filter attenuates the
253.7nm Hg line and fluoresces from 300-400 nm; and the 6057 Glass Safety Filter absorbs
the 253.7 nm Hg line and attenuates the 312.6 nm line. The Aperture Shields offered
by Newport include the 6038 Pinhole Shield which has a 0.040 inch (1mm) diameter,
the 6039 Small Aperture Shield which has a 0.313 x 0.375 inch window and the 6040
Large Aperture Shield with a 0.188 x 1.50 inch window. Filters and shields can also
be obtained from Edmund Industrial Optics Inc. (Barrington, NJ). The Edmund UV Light
Shield A has a 1mm inner diameter drilled hole; Shield B has a 7.9mm x 15.9mm aperture;
and Shield C has a 4.8 mm x 38.2 mm aperture.
[0031] The orientation of the lamp can also impact upon the result obtained. Thus, in the
embodiment where a gas is subjected to a radiation source, the radiation source can
be fixed to direct the radiation directly towards, perpendicular, away or parallel
to the conduit directing the gas, or its entry or exit point. The gases can be those
discussed above or other gases, such as air or oxygen. The radiation source can be
positioned horizontally, vertically and/or at an angle above, below across from the
conduit. For example, the base of a pencil lamp (or other radiation source) can be
set at the same height of the conduit and the tip of the lamp directed or pointed
toward the conduit. Alternatively, the base of the pencil lamp (or other radiation
source) can be set at the height of the conduit and the lamp directed at a 30° (40°,
45°, 50°, 55°, 60°, or 90°) angle above (below) the conduit. Alternatively, the base
of the pencil lamp can be fixed above or below the level of the conduit. The tip of
the pencil lamp can be pointed up or down, in the direction of the gas flow or against
the gas flow or at another angle with respect to any of the above. Further, more than
one of the same or different pencil lamps alone or in combination with other radiation
sources can be used, set at the same or different heights, orientations and angles.
The lamps can be presented in alternative orders (first xenon, then mercury or vice
versa).
[0032] In an embodiment wherein the material to be treated is subjected to the radiation
source, similar positions can be achieved as above with respect to the gas conduit.
The radiation source can be fixed to direct the radiation directly towards, perpendicular,
away or parallel to the material. The radiation source can be positioned horizontally,
vertically and/or at an angle above, below across from the material. As above, the
base of a pencil lamp (or other radiation source) can be set at the same height of
the material and the tip of the lamp directed or pointed toward the material. Alternatively,
the base of the pencil lamp (or other radiation source) can be set at the height of
the material and the lamp directed at a 30° (40°, 45°, 50°, 55°, 60°, or 90°) angle
above (below) the material. Alternatively, the base of the pencil lamp can be fixed
above or below the level of the material. The tip of the pencil lamp can be pointed
up or down, in the direction of the gas flow or against the gas flow or at another
angle with respect to any of the above. Further, more than one of the same or different
pencil lamps alone or in combination with other radiation sources can be used, set
at the same or different heights, orientations and angles.
[0033] In a preferred embodiment, the radiation source is a high intensity discharge lamp
positioned to direct the radiation towards the material. The high intensity discharge
lamp is combined with one or more pencil lamps positioned proximal to the high intensity
discharge lamp. Often, high intensity discharge lamps are equipped with a hood or
reflector to direct the radiation. In some instances, one or more pencil lamps can
be placed inside and/or behind the reflector.
[0034] Further, the distance between the radiation source and the material and/or gas conduit
can impact the results achieved. For example, the lamps can be placed between about
5 and 100 cm or more from the conduit and/or material. In other embodiments, the distance
between the radiation source and the material and/or gas conduit can be between about
100 cm and 5 meters or more.
[0035] In other instances, the radiation can be filtered. Filters, such as colored glass
filters, available from photography supply shops, for example, can be used. In yet
other embodiments, the filter can be other materials, such as water, gas (air or other
gas), a manufactured or tailored material, such as those materials described or made
herein, or a material of selected density, chemical make-up, properties or structure.
In one embodiment, the filter can be placed between the radiation source(s) and the
target metal or alloy or gas used in the method. Filters can also be called "(harmonic)
forcing functions." Forcing functions can be used in conjunction with electromagnetic
radiation sources to affect a change in a material. In addition, gases may be injected
into apparatus containing a forcing function to modify the performance of the assembly.
[0036] In one embodiment, the radiation source has an environment which is different from
that of the material. This can be accomplished by directing a gas flow into the lamp
environment. Where the radiation source is a pencil lamp within a box to radiate a
gas, this can be accomplished by direct gas flow into the box. In other embodiments,
the radiation source can be a short arc lamp or a short arc lamp assembly. In such
embodiments, the gas can be introduced into the reflector proximate to the lamp. The
gas includes those gases discussed above.
[0037] The radiation can be applied continuously or discontinuously (e.g. pulsed or toggled)
and its intensity can be modulated. Where the radiation is applied continuously, the
radiation can begin prior to introduction of the gas into the conduit or after. It
can be applied for the duration of a cycle or series of cycles. Where the radiation
is pulsed, the length of each pulse can be the same or different. Generally, the radiation
is applied to induce harmonic change, altering the gas or target materials prior to
their introduction into the reactor. This is conveniently accomplished by controlling
the lamps with a computer. The factors to be considered in radiation source placement,
exposure and sequence include the desired wavelength, intensity, and energy characteristics,
the angle of incidence, and the harmonic profile to be injected into the targeted
material (e.g. gas, metal, tailored metal, radiated gas and the like).
[0038] In some instances, the radiation source and/or pencil lamp(s) and/or filters and/or
target material or gas are advantageously cooled. For example, where a high intensity
discharge lamp is used in combination with a pencil lamp(s), it may be advantageous
to cool the pencil lamp to prevent damage. Alternatively, where a short arc lamp is
used in combination with pencil lamps and/or glass filters it may be advantageous
to cool the pencil lamps to prevent damage as well as the glass filter to prevent
breakage.
[0039] Other sources of energy can be used to further tailor the materials of the invention.
For example, DC current can be applied continuously or the amperage varied, for example
between 0-300 amps, such as 0-150 amps. AC current can be applied continuously or
varied, e.g., in a wave pattern, such as a sinusoidal wave, square wave, or triangle
wave pattern of a selected frequency and amplitude. Typically, 10 volts, peak to peak,
is used at 0-3.5 MHz, 0-28 MHz, or 0-50 MHz. In other embodiments, the peak to peak
voltage was less that about 15 vdc, 10 vdc, 8 vdc, 7.2 vdc, 5 vdc, 1.7 vdc, and 1
vdc. In one embodiment, electrodes can be placed in the reactor, such as below the
surface of the material, and current applied. As with the radiation discussed above,
the current can be applied to coincide with a cycle or series of cycles or during
all or a part of a single step of the process. Often the power supply is turned on
prior to attachment to the electrodes to avoid any power surge impacts.
[0040] Further, the cooling step can alter the results of the process. Such cooling can
include gradual and/or rapid cooling steps. Gradual cooling typically includes cooling
due to heat exchange with air or other gas over 1 to 72 hours, 2 to 50 hours, 3 to
30 hours, or 8 to 72 hours. Rapid cooling, also known as quenching, typically includes
an initial cooling with air or other gas to below the solidus temperature, thereby
forming a solid mass, and placing the solid mass into a bath comprising a suitable
fluid such as tap water, distilled water, deionized water, other forms of water, gases
(as defined above), liquid nitrogen or other suitable liquified gases, a thermally-stable
oil (e.g., silicone oil) or organic coolant, and combinations thereof. The bath should
contain a suitable quantity of liquid at a suitable temperature, such that the desired
amount of cooling occurs. The ingot can be removed from the crucible before or after
completing the cooling. While the material is cooling, the environment can be stirred,
mixed or agitated. This can be accomplished by maintaining a flow of coolant over
the material, or agitating the cooling bath or environment. Alternatively, the coolant
is not disturbed or agitated and circulation of the coolant is minimized.
[0041] In one embodiment, the material is cooled in a different vessel (cooling or quench
chamber). The cooling chamber can be, for example, a polyethylene (or other plastic)
container. The ingot can be placed directly, or indirectly, into the cooling vessel
(e.g., in a vertical or horizontal orientation). Generally, the ingot can be placed
at least about 6 inches from the inside wall of the container. The height of the coolant
can be at least about 12 inches above and below the surface of the ingot. A refractory
material (e.g., a ceramic block rinsed with coolant (e.g., DI water) and, optionally
dried or allowed to dry) may be used to support the ingot in the quench chamber.
[0042] Where the material is cooled in a different vessel from the reactor or induction
furnace, the material can be removed, manually or robotically, to a clean, protected
surface. This removal may be accomplished manually using a pair of tongs (e.g. cast
iron, steel, stainless steel, nickel, titanium, tungsten or other high temperature
melting transition metal). Manual removal can also be accomplished by donning heavy,
insulated, heat resistant gloves.
[0043] Where the crucible is removed from the reactor with the material, the crucible should
be removed before or after cooling. The crucible can be removed by gently peeling
it away from the material. A hammer, ram or wedge can be used to perform this function.
However, care should be used to avoid striking the material hard with the hammer or
otherwise causing a substantial impact upon or metal contact with the material. In
one embodiment, the crucible removal can be performed in the presence of air at about
350±75°F, 750±250°F, 1100±250°F, or at T
solidus -75°F, T
solidus -5°F.
[0044] One example of the base method can be described in terms of carbon saturation values.
After a metal or alloy is added to a suitable reactor, establish the dissolved carbon
level at 70% to 95% of the equilibrium saturation of carbon for the thermodynamic
state specified (e.g., T, P, composition) when the composition is in its natural state
(hereinafter the equilibrium saturation of carbon is referred to as "[C]
eqsat"). Identify temperature set points for 80% and 95% [C]
eqsat. Vary the temperature between the predetermined set points, such that the temperature
is decreased for 7 minutes and increased over 7 minutes per cycle, for 15 cycles.
Next, establish a flow of argon. Vary the temperature between the predetermined set
points, such that the temperature is decreased for 7 minutes and increased over 7
minutes per cycle, for 5 cycles; the temperature should be maintained above 70% [C]
eqsat at all times and maintained below 95% [C]
eqsat at all times. The carbon level is raised to saturation (i.e., [C]
eqsat) with continued argon addition. Hold for 60 minutes at saturation (i.e., [C]
eqsat) with continued argon addition. Raise the carbon level to
+1%
wt (i.e.,
+1%
wt represents 1%
wt above the saturation value as defined in its natural equilibrium state, [C]
eqsat) of [C]
eqsat with continued argon addition and hold for 5 minutes. Vary the temperature for 20
cycles between
+1%
wt and
+3%
wt of [C]
eqsat, such that the temperature is decreased over 9 minutes and increased over 9 minutes
per cycle. Cease argon addition. Cool the metal to
+4%
wt of [C]
eqsat. Vary the temperature for 4.5 cycles between
+4%
wt and
+7%
wt of [C]
eqsat, such that the temperature is decreased over 3 minutes and increased over 5 minutes.
Argon is added as the carbon saturation increases and nitrogen is added as carbon
saturation decreases. Cool the metal to obtain
+8%
wt with continued argon addition. Vary the temperature over 15.5 cycles between
+8%
wt and
+18%
wt of [C]
eqsat, such that the temperature is decreased over 15 minutes and increased over 15 minutes.
Argon is added as the carbon saturation increases and nitrogen is added as carbon
saturation decreases. After the 15.5 cycles are complete, gas addition is halted.
Perform one complete cycle by varying the temperature between
+18%
wt to
+14%
wt of [C]
eqsat (ending at
+18%
wt), such that the temperature is increased over 15 minutes and decreased over 15 minutes.
Proceed immediately to a cool down that leads to solidification. The present process
also includes one or more of the further improvements described above.
[0045] Cycles of the present invention can vary in duration. The duration of a cycle can
vary among cycles in a step. A cycle duration is, for example, about 2 minutes to
about 90 minutes, about 3 minutes to about 67 minutes, about 5 minutes to about 45
minutes, about 8 minutes to about 30 minutes, about 10 minutes to about 20 minutes,
about 14 minutes to about 18 minutes, about 7 minutes to about 9 minutes, about 13
minutes to about 15 minutes, about 17 minutes to about 19 minutes, about 28 minutes
to about 32 minutes, or about 29 minutes to about 31 minutes.
[0046] A cycle can be symmetric or asymmetric. In a symmetric cycle, the period of increasing
the metal or alloy temperature is equal to the period of decreasing the metal or alloy
temperature. In an asymmetric cycle, the period of increasing the metal or alloy temperature
is different than the period of decreasing the metal or alloy temperature. For an
asymmetric cycle, the period of increasing the metal or alloy temperature can be longer
than or shorter than the period of decreasing the metal or alloy temperature.
[0047] For example, in a cycle lasting about 7 minutes to about 9 minutes, the temperature
can be increased for about 3 minutes and the temperature can be decreased for about
5 minutes. If the cycle lasts about 13 minutes to about 15 minutes, the temperature
can be increased for about 7 minutes and the temperature can be decreased for about
7 minutes. If the cycle lasts about 17 minutes to about 19 minutes, the temperature
can be increased for about 9 minutes and the temperature can be decreased for about
9 minutes. If the cycle lasts about 29 minutes to about 31 minutes, the temperature
can be increased for about 15 minutes and the temperature can decreased for about
15 minutes.
[0048] The number of cycles in a step is generally an integer or half-integer value. For
example, the number of cycles in a step can be one or more, one to forty, or one to
twenty. The number of cycles can be 1, 2, 3, 4, 5, 6, 7, 8, 9, 10, 11, 12, 13, 14,
15, 16, 17, 18, 19, 20, 21, 22, 23, 24, 25, 26, 27, 28, 29, 30, 31, 32, 33, 34, 35,
36, 37, 38, 39, or 40 or more. Alternatively, the number of cycles in a step can be
0.5, 1.5, 2.5, 3.5, 4.5, 5.5, 6.5, 7.5, 8.5, 9.5, 10.5, 11.5, 12.5, 13.5, 14.5, 15.5,
16.5, 17.5, 18.5, 19.5, 20.5, 21.5, 22.5, 23.5, 24.5, 25.5, 26.5, 27.5, 28.5, 29.5,
or 30.5 or more. In a step comprising a half-integer or a non-integer quantity of
cycles, either heating or cooling can occur first.
[0049] After the initial heating step, the temperature of a metal or an alloy is sufficiently
high, such that the temperature is equal to or greater than the solidus temperature.
The solidus temperature varies depending on the metal or the alloy, and the amount
of carbon dissolved therein. The temperature at the end of Step (F.) of the third
paragraph of the summary is typically about 900°F to about 3000°F, but varies from
metal to metal. For example, the temperature at the end of Step (F.) can be about
1932°F to about 2032°F, about 1957°F to about 2007°F, or about 1932°F to about 2467°F
for copper; about 2368°F to about 2468°F, about 2393°F to about 2443°F, or about 2368°F
to about 2855°F for nickel; about 2358°F to about 2458°F or about 2373°F to about
2423°F, or about 2358°F to about 2805°F for cobalt; about 1932°F to about 2032°F,
about 1957°F to about 2007°F, or about 1932°F to about 2467°F for a copper/gold/silver
alloy; about 399°F to about 499°F, about 424°F to about 474°F, or about 399°F to about
932°F for a tin/lead/zinc alloy; about 399°F to about 499°F, about 424°F to about
474°F, or about 399°F to 932°F for a tin/sodium/potassium/magnesium alloy; about 2550°F
to about 2650°F, about 2575°F to about 2625°F, or about 2550°F to about 2905°F for
silicon; about 2058°F to about 2158°F, about 2073°F to about 2123°F, or about 2058°F
to about 2855°F for iron; about 2058°F to about 2158°F, about 2073°F to about 2123°F,
or about 2058°F to about 2855°F for an iron/vanadium/chromium/manganese alloy; or
2368°F to about 2468°F, about 2393°F to about 2443°F, or about 2368°F to about 2855°F
for a nickel/tantalum/hafnium/ tungsten alloy.
[0050] Methods of the present invention are carried out in a suitable reactor. Suitable
reactors are selected depending on the amount of metal or alloy to be processed, mode
of heating, extent of heating (temperature) required, and the like. A preferred reactor
in the present method is an induction furnace reactor, which is capable of operating
in a frequency range of 0 Hz to about 10,000 Hz, 0 Hz to about 3,000 Hz, or 0 Hz to
about 1,000 Hz. Reactors operating at lower frequencies are desirable for larger metal
charges, such that a reactor operating at 0-3,000 Hz is generally suitable for 20
pound metal charges and a reactor operating at 0-1,000 Hz is generally suitable for
5000 pound metal charges.
[0051] Typically, reactors of the present method are lined with a suitable crucible and
appropriately sealed from the external environment enabling very tight control of
the internal chemical environment (e.g., part per thousand, part per million, or the
like). Crucibles are selected, in part, based on the amount of metal or alloy to be
heated and the temperature of the method. Crucibles selected for the present method
typically have a capacity from about five pounds to about five tons. One preferred
crucible is comprised of 89.07% Al
2O
3, 10.37% SiO
2, 0.16% TiO
2, 0.15% Fe
2O
3, 0.03% CaO, 0.01% MgO, 0.02% Na
2O
3, and 0.02% K
2O, and has a 9 inch outside diameter, a 7.75 inch inside diameter, and a 14 inch depth.
A second preferred crucible is comprised of 99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, and 0.12% Na
2O
3, and has a 4.5 inch outside diameter, a 3.75 inch inside diameter and a 10 inch depth.
[0052] A new composition of matter of the present invention can manifest itself as a transient,
adjustable, or permanent change in energy and/or associated properties, as broadly
defined. Property change can be exhibited as or comprise a change in: (1) structural
atomic character (e.g., XES/XRF peak creation, peak fluidity, peak intensity, peak
centroid, peak profile or shape as a function of material/sample orientation, atomic
energy level(s), and TEM, STM, MFM scans); (2) electronic character (e.g., SQUID,
scanning SQUID,scanning magnetoresistive microscopy, scanning magnetic microscope,
magnetometer, non-contact MFM, electron electromagnetic interactions, quantum (or
topological) order
1,2, quantum entanglement
3, Jahn-Teller effect, ground state effects, electromagnetic field position/orientation,
energy gradients, Hall effect, voltage, capacitance, voltage decay rate, voltage gradient,
voltage signature including slope of decay and/or change of slope decay, voltage magnitude,
voltage orientation); (3) structural molecular or atomic character (e.g., SEM, TEM,
STM, AFM, LFM, and MFM scans, optical microscopy images, and structural orientation,
ordering, long range alignment/ordering, anisotropy); (4) physical constants (e.g.,
color, crystalline form, specific rotation, emissivity, melting point, boiling point,
density, refractive index, solubility, hardness, surface tension, dielectric, magnetic
susceptibility, coefficient of friction, x-ray wavelengths); (5) physical properties
(e.g., mechanical, chemical, electrical, thermal, engineering, and the like); and,
(6) other changes that differentiate naturally occurring materials from manufactured
materials created by inducing a change in matter.
[0053] A preferred analytical method is x-ray fluorescence spectrometry. X-ray fluorescence
spectrometry is described in "
X-Ray Fluorescence Spectrometry", by George J. Havrilla in "Handbook of Instrumental
Techniques for Analytical Chemistry," Frank A. Settle, Ed., Prentice-Hall, Inc: 1997, which is incorporated herein by reference. XRF spectrometry is a well-known and
long-practiced method, which has been used to detect and quantify or semi-quantify
the elemental composition (for elements with Z ≥ 11) of solid and liquid samples.
This technique benefits from minimal sample preparation, wide dynamic range, and being
nondestructive. Typically, XRF data are not dependent on which dimension (e.g., axial
or radial) of a sample was analyzed. Accuracy of less than 1% error can generally
be achieved with XRF spectrometry, and the technique can have detection limits of
parts per million.
[0054] XRF spectrometry first involves exciting an atom, such that an inner shell electron
is ejected. Upon ejection of an electron, an outer shell electron will "drop" down
into the lower-energy position of the ejected inner shell electron. When the outer
shell electron "drops" into the lower-energy inner shell, x-ray energy is released.
Typically, an electron is ejected from the K, L, or M shell and is replaced by an
electron from the L, M, or N shell. Because there are numerous combinations of ejections
and replacements possible for any given element, x-rays of several energies are emitted
during a typical XRF experiment. Therefore, each element in the Periodic Table has
a standard pattern of x-ray emissions after being excited by a sufficiently energetic
source, since each such element has its own characteristic electronic state. By matching
a pattern of emitted x-ray energies to values found in tables, such as those on pages
10-233 to 10-271 of "Handbook of Chemistry and Physics, 73rd Edition," edited by D.
R. Lide, CRC Press, 1992, which is incorporated herein by reference, one can identify which elements are present
in a sample. In addition, the intensity of the emitted x-rays allows one to quantify
the amount of an element in a sample.
[0055] There are two standard variations of the XRF technique. First, as an energy-dispersive
method (EDXRF), the XRF technique uses a detector such as a Si(Li) detector, capable
of simultaneously measuring the energy and intensity of x-ray photons from an array
of elements. EDXRF is well-suited for rapid acquisition of data to determine gross
elemental composition. Typically, the detection limits for EDXRF are in the range
of tens to hundreds of parts-per-million. A wavelength-dispersive technique (WDXRF)
is generally better-suited for analyses requiring high accuracy and precision. WDXRF
uses a crystal to disperse emitted x-rays, based on Bragg's Law. Natural crystals,
such as lithium fluoride and germanium, are commonly used for high-energy (short wavelength)
x-rays, while synthetic crystals are commonly used for low-energy (longer wavelength)
x-rays. Crystals are chosen, in part, to achieve desired resolution, so that x-rays
of different energies are dispersed to distinguishable 2θ angles. WDXRF can either
measure x-rays sequentially, such that a WDXRF instrument will step through a range
of 2θ angles in recording a spectrum, or there will be detectors positioned at multiple
2θ angles, allowing for more rapid analysis of a sample. Detectors for WDXRF commonly
include gas ionization and scintillation detectors. A further description of the use
of WDXRF technique in the present invention can be found in Example 1. Results from
EDXRF and results from WDXRF can be compared by determining the relationship between
a 2θ angle and the wavelength of the corresponding x-ray (e.g., using Bragg's Law)
and converting the wavelength into energy (e.g., energy equals the reciprocal of the
wavelength multiplied by Planck's constant and the velocity of light).
[0056] Analysis of emitted x-rays can be carried out automatically or semiautomatically,
such as by using a software package (e.g., UniQuant, which is sold by Omega Data Systems
BV, Veldhoven, The Netherlands) for either EDXRF or WDXRF. UniQuant is used for standard-less,
semi-quantitative to quantitative XRF analysis using the intensities measured by a
sequential x-ray spectrometer. The software package unifies all types of samples into
one analytical program. The UniQuant software program is highly effective for analyzing
samples for which no standards are available. Sample preparation is usually minimal
or not required at all. Samples can be of very different natures, sizes and shapes.
Elements from fluorine or sodium up to uranium, or their oxide compounds, can be analyzed
in samples such as a piece of glass, a screw, metal drillings, lubricating oil, loose
fly ash powder, polymers, phosphoric acid, thin layers on a substrate, soil, paint,
the year rings of trees, and, in general, those samples for which no standards are
available. The reporting is in weight % along with an estimated error for each element.
[0057] In software packages such as UniQuant, an XRF spectrum is composed of data channels.
Each data channel corresponds to an energy range and contains information about the
number of x-rays emitted at that energy. The data channels can be combined into one
coherent plot to show the number or intensity of emitted x-rays versus energy or 2θ
angle (the 2θ angle is related to the wavelength of an x-ray), such that the plot
will show a series of peaks. An analysis of the peaks by one skilled in the art or
the software package can identify the correspondence between the experimentally-determined
peaks and the previously-determined peaks of individual elements. For an element,
peak location (i.e., the centroid of the peak with respect to energy or 2θ angle),
peak profile/ shape, peak creation, and peak fluidity would be expected to be essentially
the same, within experimental error, for any sample containing the element. If the
same quantity of an element is present in two samples, intensity will also be essentially
the same, excepting experimental error and matrix effects.
[0058] A typical software package is programmed to correlate certain data channels with
the emitted x-rays of elements. Quantification of the intensity of emitted x-rays
is accomplished by integrating the XRF spectrum over a number of data channels. Based
on the measured intensities and the previously-compiled data on elements, the software
package will integrate over all data channels, correlate the emitted x-ray intensities,
and will then calculate the relative abundance or quantity of elements which appear
to be present in a sample, based upon comparison to the standards. Composition of
matter changes produced by the present invention will generally be characterized by
an XRF spectrum that reports: (1) the presence of an element which was not present
in the starting material and was not added during the process; (2) an increased amount
of an element that was not added to the process in the amount measured; or, (3) a
decreased amount of an element that was not removed during the process in the amount
indicated. Examples of (3) include a reduction in identifiable spectra referencing
the sum before normalization and/or reappearance of an element upon combustion. Products
of the present invention can also be characterized by the difference between XRF Uniquant
analysis such as by burning the sample (e.g., LECO analysis), described in more detail
below.
[0059] A "LECO" analysis is meant to include an analysis conducted by the CS-300 Carbon/Sulfur
determinator supplied by a LECO computer. The CS-300 Carbon/Sulfur determinator is
a microprocessor based, software driven instrument for measurement of carbon and sulfur
content in metals, ores, ceramics and other inorganic materials.
[0060] Analysis begins by weighing out a sample (1 g nominal) into a ceramic crucible on
a balance. Accelerator material is added, the crucible is placed on the loading pedestal,
and the ANALYZE key is pressed. Furnace closure is performed automatically, then the
combustion chamber is purged with oxygen to drive off residual atmospheric gases.
After purging, oxygen flow through the system is restored and the induction furnace
is turned on. The inductive elements of the sample and accelerator couple with the
high frequency field of the furnace. The pure oxygen environment and the heat generated
by this coupling cause the sample to combust. During combustion all elements of the
sample oxidize. Carbon bearing elements are reduced, releasing the carbon, which immediately
binds with the oxygen to form CO and CO2, the majority being CO2. Also, sulfur bearing
elements are reduced, releasing sulfur, which binds with oxygen to form SO
2.
[0061] Sample gases are swept in the carrier stream. Sulfur is measured as sulfur dioxide
in the first IR cell. A small amount of carbon monoxide is converted to carbon dioxide
in the catalytic heater assembly while sulfur trioxide is removed from the system
in a cellulose filter. Carbon is measured as carbon dioxide in the IR cells, as gases
flow trough the IR cells.
[0062] Ideally, the relative abundances will total 100% prior to normalization. However,
for a variety of reasons, such as improper or insufficient calibration, and/or non-planar
sample surface the relative abundances will not total 100% prior to normalization.
Another reason that the relative abundances of elements do not total 100% prior to
normalization is that a portion of the XRF spectrum falls outside of the data channels
that the software package correlates with an element (i.e., a portion of the XRF spectrum
is not recognized as belonging to an element and is not included in the relative abundance
calculation). In this case, the relative abundances will likely total less than 100%
prior to normalization. Further, the samples will often have anisotropic characteristics
whereby an axial scan is distinct from a radial scan. Thus, products of the invention
may be characterized by an XRF spectrum that is not recognized by the Uniquant software
(e.g., sum of known concentrations before normalization is less than 100%) described
herein in an amount, for example, of less than 98%, such as less than 90%, such as
less than 80%. In additional embodiments, the software package reports or detects
one or more elements not detected by other methods or are detected in different quantities.
[0063] X-ray emission spectrometry (XES), a technique analogous to XRF, also provides electronic
information about elements. In XES, a lower-energy source is used to eject electrons
from a sample, such that only the surface (to several micrometers) of the sample is
analyzed. Similar to XRF, a series of peaks is generated, which corresponds to outer
shell electrons replacing ejected inner shell electrons. The peak shape, peak fluidity,
peak creation, peak intensity, peak centroid, and peak profile are expected to be
essentially the same, within experimental error and matrix effects, for two samples
having the same composition.
[0064] Thus, XES analysis of the control standard compared to the atomically altered (i.e.,
manufactured or tailored) state can also be analyzed. Manufactured copper in the axial
direction exhibits similar composition to natural copper (i.e., 99.98%
wt), but radial scans exhibit new peaks in the region close to naturally occurring S,
Cl, and K. The shifting centroid of the observed peaks from the natural species (i.e.,
S, Cl, and K) confirms electronic change in the atomic state of the base element.
Conventional chemical analysis performed using a LECO (IR) analyzer to detect SO
x in the vapor phase post sample combustion confirmed the absence of sulfur at XES
lower detection limits.
[0065] Non-contact, magnetic force microscopy image or scanning tunneling microscopy (STM)
scan can also confirm the production of a new composition of matter or manufactured
or tailored material, identified by an altered and aligned electromagnetic network.
Individually, and from differing vantage points, these scans show the outline of the
changed electromagnetic energy network.
[0066] New compositions of matter can be electronically modified to induce long range ordering/alignment.
Optical microscopy and SEM imaging of the material verifies the degree and extent
of long range ordering achieved.
[0067] Non-contact, magnetic force microscopy image or scanning tunneling microscopy (STM)
scans can also confirm the production of a new composition of matter or manufactured
or tailored material, identified by an altered and aligned electromagnetic network.
Individually, and from differing vantage points, these scans can show the outline
of the changed electromagnetic energy network. Non-contact MFM imaging can show that
products of the invention often possess clear pattern repetition and intensity of
the manufactured material when compared to the natural material, or starting material.
Products of the invention can be characterized by the presence of magnetic properties
in high purity, non-magnetic metals, such as elemental copper (e.g., 99.98 %
wt).
[0068] Products can also be characterized by color changes. The variation in color of copper
products ranged from black, copper, gold, silver and red. Other visual variations
included translucency and near transparency at regions. While not being bound by theory,
the alteration of copper's electronic state along the continuum enables the new composition
of matter's color to be adjusted along the continuum.
[0069] In several examples of the present invention, the ingots obtained by the process
possess a substantial internal void and absence of a crown of material on the top
surface. In other examples of the invention, the ingot is characterized by essentially
no void, with a crown of material on the top.
[0070] Other products of the processes are characterized by changes in hardness. The variation
in diamond pyramid hardness between different manufactured copper samples ranged from
about 25 to 90 (or 3 to 9 times higher than natural copper). Hardness change can be
anisotropic.
[0071] The operations described in the embodiments presented herein did not result merely
from empirical explorations. Rather, guidance was obtained from theoretical considerations
regarding the topological aspects of electrodynamics. These enabled specification
of the range and duration of temperature cycles, the selection of specific combinations
and concentrations of gases to be used, geometric factors affecting the lance placement,
and all other chief features of the experimental protocols. While not being bound
by theory, the Applicant believes the application of topological principles
4,5,6,7,8,9,10 when applied to electrodynamics provides a powerful means for altering the properties
of materials.
[0072] As noted in
US.09/416,720, the theoretical analysis can be formulated in terms of an allowed set of mathematical
poles, defined as the zurn operator, and further characterized by the set of mathematical
poles coalesced, defined as the isozurn value. Adjusting or manipulating the zurn
causes the isozurn value to differ from its starting or naturally occurring value,
thereby modifying the electronic structure from that of the natural state.
[0073] The products produced by the process have utilities readily apparent to those skilled
in the art. Indeed, materials which comprise metals can be used to manufacture products
having adjustable chemical properties (e.g., regioselectivity, regiospecificity, or
reaction rate), electronic properties (e.g., band gap, susceptibility, resistivity,
or magnetism), mechanical properties (e.g., ductility or hardness) and/or optical
properties (e.g., color).
[0074] The invention further relates to the apparatus used to produce the materials. The
apparatus of the invention includes a reactor comprising an induction furnace characterized
by a gas source and at least one radiation source arranged to expose the gas and/or
the contents of the reactor, in the manner discussed above, optional filters and optional
environmental controls. As such, the invention includes an apparatus comprising a
combination of the following: (a) a first and a second pencil lamp; (b) at least one
short arc lamp within a housing; (c) a gas source proximal to (b) and an induction
furnace.
[0075] In one embodiment, the radiation source is proximate to a gas source which is adapted
to control the environment of the radiation source. In another embodiment, the short
arc lamp housing further comprises at least one pencil lamp, such as those discussed
above. In another embodiment, the apparatus further comprises a filter, such as those
described herein.
EXEMPLIFICATION
EXAMPLE 1:
EXPERIMENTAL PROCEDURE FOR COPPER Method "AB" RUN 14-03-02
[0076] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply was charged
with 9080 g copper (99.98% purity) through its charging port. Prior to charging a
gas addition lance was placed inside the reactor at the reactor centerline and placed
two inches from the bottom of the bath. The reactor was fitted with a graphite cap
and a ceramic liner (i.e., the crucible, from Engineering Ceramics). During the entire
procedure, a slight positive pressure of 97% argon and 3% hydrogen (~0.5 psig) was
maintained in the reactor using a continuous backspace purge. The reactor was heated
to the metal charge liquidus point plus at least 300°F, at a rate no greater than
300°F/hr, as limited by the integrity of the crucible. The induction furnace operated
in the frequency range of 0 Hz to 3000 Hz, with frequency determined by a temperature-controlled
feedback loop implementing an Omega Model CN3000 temperature controller. The temperature
was increased to 2462°F again using a rate no greater than 300°F/hour. When this temperature
was reached, graphite saturation assemblies (3/8 inches OD, 36 inches long high purity
(<5 ppm impurities) graphite rods) were inserted to the bottom of the copper charge
through ports located in the top plate. The copper was held at 2462°F for 2 hours.
Every 30 minutes during the hold period, an attempt was made to lower the graphite
saturation assemblies as dissolution occurred. As the copper became saturated with
carbon, the graphite saturation assemblies were consumed. After the 2-hour hold period
was complete, the graphite saturation assemblies were removed.
[0077] The reactor temperature was increased to 2515°F over 7 minutes. The temperature was
then varied between 2476°F and 2515°F for 16.5 cycles. Each cycle consisted of raising
the temperature continuously over 7 minutes and lowering the temperature continuously
over 7 minutes. After the 15 cycles were completed, the gas flow rate was started
in a bypass mode at a rate of 0.3 L/min of 97% argon and 3% neon (all gas compositions
are constant unless stated otherwise). Five minutes into the 15.5
th cycle, a xenon radiation source is activated within the sealed enclosure. At 6 minutes
into the 15.5
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, the gas flow was redirected to direct bath addition. At sweep
count 16, a short wave ultraviolet radiation source was initiated in the sealed enclosure.
At sweep count 16.5, the xenon radiation source was remotely rotated within the sealed
enclosure. The temperature of the copper was varied over another 5 cycles between
2476°F and 2515°F. After the fifth cycle, the reactor temperature was lowered to 2462°F
over a 10-minute period.
[0078] The graphite saturation assemblies were reinstalled in the copper and remained there
for 1 hour. The graphite saturation assemblies were removed. The reactor temperature
was lowered to 2459°F over 5 minutes. The reactor was held at this temperature for
5 minutes with continued gas addition. The temperature was then varied between 2453°F
and 2459°F over 20 cycles. Each cycle consisted of lowering the temperature continuously
over 9 minutes and raising the temperature continuously over 9 minutes. After the
20
th cycle, third body addition (gas addition) was changed to a flow rate of 9 mL/min
of 100% neon. The bath was then cooled to 2450°F over 10 minutes.
[0079] The temperature was then varied between 2441°F and 2450°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 40%helium, 60% argon and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 40% argon, 60% helium, trace neon, trace hydrogen,
and trace krypton was added. After the 4.5 cycles, the short wave radiation source
within the sealed enclosure was terminated. The reactor temperature was then lowered
to 2438°F over 1 minute. The temperature was varied between 2406°F and 2438°F for
15.5 cycles. Each cycle consisted of lowering the temperature continuously over 15
minutes and raising the temperature continuously over 15 minutes. In addition, while
raising the temperature, a 0.15 L/min flow of 40%helium, 60% argon and trace neon
was added, and while lowering the temperature, a 0.3 L/min flow of 40% argon, 60%
helium, trace neon, trace hydrogen, and trace krypton was added. After the final cycle
(sweep), gas flow was changed to trace neon only.
[0080] The temperature was then varied between 2419°F and 2406°F for one cycle. The cycle
consisted of raising the temperature continuously over 15 minutes and lowering the
temperature continuously over 15 minutes. At the completion of this temperature sweep,
the reactor temperature was lowered to T
solidus plus 11°F over 45 minutes.
[0081] Upon reaching T
solidus plus 11°F, gas addition was changed to 0.3 L/min of 100% hydrogen and trace neon
and held for five minutes. The reactor was then cooled to T
solidus plus 10°F over five minutes. Upon reaching T
solidus plus 10°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch (1/4 inches) dimple could be observed on the bath surface.
The bath was held at T
solidus plus 10°F for an additional 5 minutes for conditioning and equilibrization. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. Furthermore, immediately following the manual power
pulse the gas flow rate was changed to 0.15 L/min of 49.5% hydrogen, 49.5% helium
and 1% neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the reactor temperature was lowered to T
solidus minus 75°F over five hours. Upon reaching T
solidus minus 75°F, the flow rate was changed to 30 ml/min of 60% helium, 40% hydrogen and
trace neon. The induction furnace power supply was then lowered to 0.75 kW and the
reactor was allowed to cool to 1000°F. Upon reaching 1000°F, the flow rate was changed
to 30 ml/min of 100% helium and trace neon. The induction furnace power supply was
lowered to 0.50 kW and the reactor was allowed to cool to 350°F. Upon reaching 350°F,
the induction furnace power supply was shut down. A timer was initiated. At a time
of 5 minutes, the long wave radiation source within the sealed enclosure was terminated.
At a time of 9 minutes, the xenon radiation source within the sealed enclosure was
terminated. At a time of 15 minutes, the trace neon gas addition was terminated. At
a time of 30 minutes, the helium gas addition was terminated. At a time of 45 minutes,
the ingot and crucible were removed from the reactor in the presence of radiation
sources (metal halide light sources) utilizing tongs.
[0082] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing water, ensuring that the top of the ingot surface was covered by at least
6 inches of water. The ingot was allowed to stay in the quench vessel for 6 hours
prior to its removal from the quench vessel.
[0083] Note: An identical experimental program except for the use of pencil lamps -- which
provided a source of electromagnetic radiation to the third-body gases -- was also
performed verifying the efficacy of the improved process (See 14-03-03 in Table 1
and attending discussions).
EXAMPLE 2:
EXPERIMENTAL PROCEDURE FOR COPPER Method "HA" RUN 14-02-06
[0084] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductortherm) fitted with a 73-30R Powertrak power supply was charged
with 9080 g copper (99.98% purity) through its charging port. The reactor was fitted
with a graphite cap and a ceramic liner (i.e., the crucible, from Engineering Ceramics).
During the entire procedure, a slight positive pressure of nitrogen (~0.5 psig) was
maintained in the reactor using a continuous backspace purge. The reactor was heated
to the metal charge liquidus point plus at least 300°F, at a rate no greater than
300°F/hr, as limited by the integrity of the crucible. The induction furnace operated
in the frequency range of 0 Hz to 3000 Hz, with frequency determined by a temperature-controlled
feedback loop implementing an Omega Model CN3000 temperature controller. The temperature
was increased to 2462°F again using a rate no greater than 300°F/hour. When this temperature
was reached, graphite saturation assemblies (3/8 inch OD, 36 inch long high purity
(<5 ppm impurities) graphite rods) were inserted to the bottom of the copper charge
through ports located in the top plate. The copper was held at 2462°F for 2 hours.
Every 30 minutes during the hold period, an attempt was made to lower the graphite
saturation assemblies as dissolution occurred. As the copper became saturated with
carbon, the graphite saturation assemblies were consumed. After the 2 hour hold period
was complete, the graphite saturation assemblies were removed.
[0085] The reactor temperature was increased to 2539°F over 14 minutes. At this point, a
gas addition lance was lowered into the molten metal to a position approximately 2
inches from the bottom of the reactor and a 4.8 L/min flow of gas was begun. The gas
composition was 92% argon, 3% neon, and 5% helium. The temperature was then lowered
to 2515°F over 10 minutes. Flow rate was then lowered to 2.4 L/min with the same ratio
of gases (argon, neon, and helium). The temperature was then varied between 2476°F
and 2515°F for 15 cycles. Each cycle consisted of raising the temperature continuously
over 7 minutes and lowering the temperature continuously over 7 minutes. After the
15 cycles were completed, the gas flow rate was altered again to 1.4 L/min (all gas
compositions are constant unless stated otherwise). The temperature of the copper
was varied over another 5 cycles between 2476°F and 2515°F. After the fifth cycle,
the reactor temperature was lowered to 2462°F over a 30 minute period with a lowered
gas addition rate of 0.8 L/min.
[0086] The graphite saturation assemblies were reinstalled in the copper and remained there
for 1 hour. The graphite saturation assemblies were removed. Flow rate was increased
to 1.2 L/min. The reactor temperature was lowered to 2459°F over 5 minutes. The reactor
was held at this temperature for 5 minutes with continued gas addition. The temperature
was then varied between 2453°F and 2459°F over 20 cycles. Each cycle consisted of
lowering the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. During the temperature lowering portion of the cycle, gas addition
was at the rate of 1.4 L/min with a gas composition of 95% argon, 3% neon, 2% krypton.
During the temperature increasing portion of the cycle, gas addition was at the rate
of 2.8 L/min with a gas composition of 95% argon, 5% neon. After the 20
th cycle, third body addition (gas addition) was changed to a flow rate of 0.15 L/min
with a gas composition of 95% helium, 5% krypton. The bath was then cooled to 2450°F
over 13 minutes.
[0087] The temperature was then varied between 2441°F and 2450°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 1.2 L/min flow of 95% helium, 5% krypton was added, and while lowering the temperature,
a 2.4 L/min flow of 95% argon, 5% neon was added. After the 4.5 cycles, the reactor
temperature was lowered to 2438°F over 1 minute. The temperature was varied between
2406°F and 2438°F for 15.5 cycles. Each cycle consisted of lowering the temperature
continuously over 15 minutes and raising the temperature continuously over 15 minutes.
In addition, while raising the temperature, a 1.2 L/min flow of 95% nitrogen, 5% helium
was added, and while lowering the temperature, a 2.4 L/min flow of 95% argon, 5% neon
was added. After the final cycle (sweep), gas flow was changed to 0.15 L/min with
a gas composition of 95% helium, 5% argon. The reactor was then held for 16 minutes
at 2406°F.
[0088] The temperature was then varied between 2419°F and 2406°F for one cycle. The cycle
consisted of raising the temperature continuously over 15 minutes and lowering the
temperature continuously over 15 minutes. In addition, while raising the temperature,
a 2.4 L/min flow of 95% helium, 5% argon was added, and while lowering the temperature,
a 1.2 L/min flow of 95% argon, 5% nitrogen was added. At the completion of this temperature
sweep, the reactor temperature was lowered to T
solidus plus 10°F.
[0089] The gas addition lance was relocated into the headspace of the reactor, such that
a quarter inch (1/4 inches) dimple could be observed on the bath surface (1.2 L/min
flow of 95% argon, 5% nitrogen). The bath was held at T
solidus plus 10°F for an additional 5 minutes for conditioning and equilibrization. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus again maintaining a temperature lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 20°F. Upon reaching T
solidus minus 20°F, the induction furnace power supply was lowered to 0.75 kW and the reactor
was allowed to cool to 1000°F. Upon reaching 1000°F, the induction furnace power supply
was lowered to 0.50 kW and the reactor was allowed to cool to 350°F. Immediately after
setting the power to 0.5 kW, the gas flow rate was changed to 0.15 L/min with a gas
composition of 95% argon, 5% nitrogen. Upon reaching 350°F, the induction furnace
power supply was shut down. Thirty minutes were allowed to pass. The ingot and crucible
were removed from the reactor using titanium metal tongs in the presence of light
supplied by metal halide ceiling lamps.
[0090] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches of DI water. Upon entrance into the quench chamber, a timer was
established. At a time of 10 hours and 30 minutes, the ingot was removed from the
quench system using the titanium metal tongs and transferred to a clean surface. Exposure
to external radiation sources included the metal halide light and placement directly
under a skylight (which added filtered sunlight to the irradiation sources). The timer
was then reset to zero. The ingot was irradiated for 10 minutes at which point an
additional radiation source (krypton lamp) was initiated. At 18 minutes, two orthogonal
fluorescent lamp racks were turned on. At 30 minutes, two angled metal halide lights
were simultaneously turned on. At this point the timer was again reset. At a time
of 6 hours, the krypton lamp, two orthogonal fluorescent lamp racks, and the two angled
metal halide lights were sequentially turned off. The timer was again reset to zero.
At a time of 6 hours, 30 minutes, normal lab lighting (metal halides) was turned off.
The timer was reset to zero. For 48 hours, the ingot was allowed to stabilize with
no manual intervention (i.e., no handling).
EXAMPLE 3:
EXPERIMENTAL PROCEDURE FOR ALUMINIUM Method "HA" RUN 14-04-02
[0091] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductortherm) fitted with a 73-30R Powertrak power supply was charged
with 4540 g Aluminum (99.99% purity) through its charging port. The reactor was fitted
with a graphite cap and a ceramic liner (i.e., the crucible, from Engineering Ceramics).
During the entire procedure, a slight positive pressure of nitrogen (~0.5 psig) was
maintained in the reactor using a continuous backspace purge. The reactor was heated
to the metal charge liquidus point plus at least 300°F, at a rate no greater than
300°F/hr, as limited by the integrity of the crucible. The induction furnace operated
in the frequency range of 0 Hz to 3000 Hz, with frequency determined by a temperature-controlled
feedback loop implementing an Omega Model CN3000 temperature controller. The temperature
was increased to 1650°F again using a rate no greater than 300°F/hour. When this temperature
was reached, graphite saturation assemblies (3/8 inch OD, 36 inch long high purity
(<5 ppm impurities) graphite rods) were inserted to the bottom of the aluminum charge
through ports located in the top plate. The aluminum was held at 1650°F for 2 hours.
Every 30 minutes during the hold period, an attempt was made to lower the graphite
saturation assemblies as dissolution occurred. As the aluminum became saturated with
carbon, the graphite saturation assemblies were consumed. After the 2 hour hold period
was complete, the graphite saturation assemblies were removed.
[0092] The reactor temperature was increased to 1690°F over 14 minutes. At this point, a
gas addition lance was lowered into the molten metal to a position approximately 2
inches from the bottom of the reactor and a 4.8 L/min flow of gas was begun. The gas
composition was 92% argon, 3% neon, and 5% helium. The temperature was then lowered
to 1678°F over 10 minutes. Flow rate was then lowered to 2.4 L/min with the same ratio
of gases (argon, neon, and helium). The temperature was then varied between 1657°F
and 1678°F for 15 cycles. Each cycle consisted of raising the temperature continuously
over 7 minutes and lowering the temperature continuously over 7 minutes. After the
15 cycles were completed, the gas flow rate was altered again to 1.4 L/min (all gas
compositions are constant unless stated otherwise). The temperature of the aluminum
was varied over another 5 cycles between 1657°F and 1678°F. After the fifth cycle,
the reactor temperature was lowered to 1650°F over a 30 minute period with a lowered
gas addition rate of 0.8 L/min.
[0093] The graphite saturation assemblies were reinstalled in the aluminum and remained
there for 1 hour. The graphite saturation assemblies were removed. Flow rate was increased
to 1.2 L/min. The reactor temperature was lowered to 1648°F over 5 minutes. The reactor
was held at this temperature for 5 minutes with continued gas addition. The temperature
was then varied between 1646°F and 1644°F over 20 cycles. Each cycle consisted of
lowering the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. During the temperature lowering portion of the cycle, gas addition
was at the rate of 1.4 L/min with a gas composition of 95% argon, 3% neon, 2% krypton.
During the temperature increasing portion of the cycle, gas addition was at the rate
of 2.8 L/min with a gas composition of 95% argon, 5% neon. After the 20
th cycle, third body addition (gas addition) was changed to a flow rate of 0.15 L/min
with a gas composition of 95% helium, 5% krypton. The bath was then cooled to 1643°F
over 13 minutes.
[0094] The temperature was then varied between 1639°F and 1643°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 1.2 L/min flow of 95% helium, 5% krypton was added, and while lowering the temperature,
a 2.4 L/min flow of 95% argon, 5% neon was added. After the 4.5 cycles, the reactor
temperature was lowered to 1637°F over 1 minute. The temperature was varied between
1620°F and 1637°F for 15.5 cycles. Each cycle consisted of lowering the temperature
continuously over 15 minutes and raising the temperature continuously over 15 minutes.
In addition, while raising the temperature, a 1.2 L/min flow of 95% nitrogen, 5% helium
was added, and while lowering the temperature, a 2.4 L/min flow of 95% argon, 5% neon
was added. After the final cycle (sweep), gas flow was changed to 0.15 L/min with
a gas composition of 95% helium, 5% argon. The reactor was then held for 16 minutes
at 1620°F.
[0095] The temperature was then varied between 1627°F and 1620°F for one cycle. The cycle
consisted of raising the temperature continuously over 15 minutes and lowering the
temperature continuously over 15 minutes. In addition, while raising the temperature,
a 2.4 L/min flow of 95% helium, 5% argon was added, and while lowering the temperature,
a 1.2 L/min flow of 95% argon, 5% nitrogen was added. At the completion of this temperature
sweep, the reactor temperature was lowered to T
solidus plus 10°F.
[0096] The gas addition lance was relocated into the headspace of the reactor, such that
a quarter inch (1/4 inches) dimple could be observed on the bath surface (1.2 L/min
flow of 95% argon, 5% nitrogen). The bath was held at T
solidus plus 10°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus again maintaining a temperature lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 20°F. Upon reaching T
solidus minus 20°F, the induction furnace power supply was lowered to 0.75 kW and the reactor
was allowed to cool to 1000°F. Upon reaching 1000°F, the induction furnace power supply
was lowered to 0.50 kW and the reactor was allowed to cool to 350°F. Immediately after
setting the power to 0.5 kW, the gas flow rate was changed to 0.15 L/min with a gas
composition of 95% argon, 5% nitrogen. Upon reaching 350°F, the induction furnace
power supply was shut down. Thirty minutes were allowed to pass. The ingot and crucible
were removed from the reactor using titanium metal tongs in the presence of light
supplied by metal halide ceiling lamps.
[0097] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches of DI water. Upon entrance into the quench chamber, a timer was
established. At a time of 10 hours and 30 minutes, the ingot was removed from the
quench system using the titanium metal tongs and transferred to a clean surface. Exposure
to external radiation sources included the metal halide light and placement directly
under a skylight (which added filtered sunlight to the irradiation sources). The timer
was then reset to zero. The ingot was irradiated for 10 minutes at which point an
additional radiation source (krypton lamp) was initiated. At 18 minutes, two orthogonal
fluorescent lamp racks were turned on. At 30 minutes, two angled metal halide lights
were simultaneously turned on. At this point the timer was again reset. At a time
of 6 hours, the krypton lamp, two orthogonal fluorescent lamp racks, and the two angled
metal halide lights were sequentially turned off. The timer was again reset to zero.
At a time of 6 hours, 30 minutes, normal lab lighting (metal halides) was turned off.
The timer was reset to zero. For 48 hours, the ingot was allowed to stabilize with
no manual intervention (i.e., no handling).
EXAMPLE 4:
EXPERIMENTAL PROCEDURE FOR COBALT, VANADIUM, RHENIUM
Method "HD" RUN 14-01-20
[0098] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply. A gas
addition lance was installed to a position approximately ¼ inches from the bottom
of the reactor. The reactor was charged with 8899 g cobalt (99.5% purity), 182 g vanadium
(99.5% purity) and 7 g rhenium (99.997% purity) through its charging port. The reactor
was fitted with a graphite cap and a ceramic liner (i.e., the crucible, from Engineering
Ceramics). During the entire procedure, a slight positive pressure of 97% argon, 3%
hydrogen (~0.5 psig) was maintained in the reactor using a continuous backspace purge.
Bypass injection of gas addition was commenced (i.e., gas flow diverted around the
reactor was initiated) at a rate of 0.15 L/min of argon. The incoming gas line for
the gas addition lance passes through a sealed, light-tight enclosure whereby irradiation
of the gas with precise radiation sources (e.g., wavelength, intensity, etc) could
be achieved. When the entire gas line had been completely purged (assuming a plug
flow model), a neon radiation source was activated within the sealed enclosure. A
timer was set to zero. Bypass flow was adjusted to 100% argon at a flow rate of 0.15
L/min with trace neon present (trace can be defined as ≤ 0.005% vol. to ≤ 5%). At
a time of 3 minutes, an argon radiation source was activated within the sealed enclosure.
After completion of another gas line purge (assuming a plug flow model), the gas line
was switched from bypass to direct injection through the gas addition lance.
[0099] The induction furnace power was then initiated. The reactor was heated to 450°F,
at a rate no greater than 300°F/hr, as limited by the integrity of the crucible. The
induction furnace operated in the frequency range of 0 Hz to 3000 Hz, with frequency
determined by a temperature-controlled feedback loop implementing an Omega Model CN3000
temperature controller. Upon reaching 450°F, the gas addition lance was repositioned
to 2 inches from the bottom of the reactor. The timer was again set to zero. At a
time of 2 minutes, the gas composition was changed to 0.15 L/min of 66% nitrogen,
34% hydrogen with trace neon present. After completion of another gas line purge (assuming
a plug flow model), a krypton radiation source was initiated in the sealed enclosure.
Continue reactor heat up at a rate no greater than 300°F/hr, as limited by the integrity
of the crucible, until T
solidus minus 30°F was achieved. The gas flow rate was then increased to 0.3 L/min with a
constant gas composition. At T
solidus a second argon radiation source was activated within the sealed enclosure. Approach
T
solidus plus 8°F over a 3 to 5 minute time span. From T
solidus plus 8°F to T
solidus plus 15°F, reduce the gas flow rate to 0.15 L/min with a constant gas composition.
Immediately upon reaching T
solidus plus 15°F, a second neon radiation source was initiated in the sealed enclosure.
Immediately after the second neon radiation source was initiated, the gas composition
was adjusted to 75% hydrogen, 22% nitrogen, 3% argon and trace neon. The molten bath
was held at this condition for 5 minute for stabilization.
[0100] After the 5 minute hold, the gas composition was adjusted to 20% helium, 63% nitrogen,
17% argon, and trace neon. The bath was held under these conditions for an additional
15 minutes. Again, following the hold, the gas composition and flow rate were adjusted
to 100% argon with trace neon at a rate of 0.3 L/min. The reactor was held at this
condition for 3 minutes. The timer was reset to zero. At a time of 65 minutes, graphite
saturation assemblies (3/8 inches OD, 36 inches long high purity (<5 ppm impurities)
graphite rods) were inserted to the bottom of the cobalt alloy charge through ports
located in the top plate. The cobalt was heated to 2504°F over a one hour period.
The bath was then held at this condition for 2 hours. Every 30 minutes during the
hold period, an attempt was made to lower the graphite saturation assemblies as dissolution
occurred. As the cobalt became saturated with carbon, the graphite saturation assemblies
were consumed. After the 2 hour hold period was complete, the graphite saturation
assemblies were removed. An additional 47 grams of graphite powder was charged into
the reactor through the charging port. The bath was then heated to 3194°F over three
hours. Upon achieving 3194°F, the gas composition and flow rate were adjusted to 100%
nitrogen with trace neon at a rate of 0.3 L/min. Hold reactor conditions for five
minutes. Reduce the gas flow rate to 0.15 L/min with constant composition. Immediately
following this reduction in gas flow, the krypton radiation source in the sealed enclosure
was turned off. The timer was reset to zero. At a time of 3 minutes, the gas flow
rate was reduced to 37.5 ml/min with constant composition. One of the argon radiation
sources inside the sealed enclosure was turned off. At a time of 5 minutes, the nitrogen
component of the gas flow was discontinued, while maintaining the flow of trace neon.
At a time of 10 minutes, remotely rotate one of the neon radiation sources within
the sealed enclosure. The reactor temperature was lowered to 3064°F over 7 minutes.
[0101] The temperature was then varied between 2851°F and 3064°F for 16 cycles. Each cycle
consisted of raising the temperature continuously over 7 minutes and lowering the
temperature continuously over 7 minutes. After completion of the 14.5 cycles, argon
was reintroduced at a flow rate of 0.15 L/min with trace neon. Five minutes into the
15
th cycle, a xenon radiation source was activated within the sealed enclosure. At 6 minutes
into the 15
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, a short wave ultraviolet radiation source was initiated in the
sealed enclosure. At sweep count 16, remotely rotate the xenon radiation source within
the sealed enclosure. The temperature of the cobalt was varied over another 5 cycles
between 2851°F and 3064°F. After the fifth cycle, the reactor temperature was lowered
to 2775°F over a 10 minute period. Upon achieving the target temperature of 2775,
the graphite saturation assemblies were reinstalled in the cobalt and remained there
for 1 hour. The graphite saturation assemblies were then removed.
[0102] Two voltage probes (source and ground probe) were then installed in the headspace
of the reactor and allowed to equilibrate for 5 minutes. Upon completion of the five
minute hold the voltage probes were lowered into the bath. The source probe should
be positioned 2 inches below the axial center and 1 inch from the radial center. The
ground probe was positioned 0.75 inches above the axial position of the source probe
and 1 inch from the radial center (180° from the source probe). Once the probes are
installed a five minute hold at this condition is done to allow the bath to electronically
equilibrate with the probes. Voltage was then applied to the probes and varied between
multiple voltage set points. This voltage application was in a continuous up/down
sweep between two predetermined voltages. The first voltage cycle was varied between
17 and 18 volts for 24 cycles. Each cycle consisted of raising the voltage continuously
over 45 seconds and lowering the voltage continuously over 45 seconds. The second
voltage cycle was varied between 13.25 and 14.75 volts for 20 cycles. Each cycle consisted
of raising the voltage continuously over 45 seconds and lowering the voltage continuously
over 45 seconds. The third voltage cycle was varied between 8.75 and 10.25 volts for
17 cycles. Each cycle consisted of raising the voltage continuously over 45 seconds
and lowering the voltage continuously over 45 seconds. The fourth voltage cycle was
varied between 4.00 and 7.00 volts for 14 cycles. Each cycle consisted of raising
the voltage continuously over 45 seconds and lowering the voltage continuously over
45 seconds. The fifth voltage cycle was varied between 1.50 and 5.00 volts for 10
cycles. Each cycle consisted of raising the voltage continuously over 45 seconds and
lowering the voltage continuously over 45 seconds. The sixth voltage cycle was varied
between 0.50 and 2.00 volts for 3 cycles. Each cycle consisted of raising the voltage
continuously over 45 seconds and lowering the voltage continuously over 45 seconds.
When the final cycle was completed the voltage was set onto a constant 1 volt setting.
This voltage remained constant until a later step during which the leads were removed.
[0103] The reactor temperature was then lowered to 2759°F over 5 minutes. The reactor was
held at this temperature for 5 minutes with continued gas addition. The temperature
was then varied between 2727°F and 2759°F over 20 cycles. Each cycle consisted of
lowering the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. After the 20
th cycle, third body gas addition was changed by turning off the argon component of
the gas leaving only trace neon gas flow. The bath was then cooled to 2711°F over
5 minutes. Upon reaching 2711°F, one of the neon radiation sources within the sealed
enclosure was remotely rotated.
[0104] The temperature was then varied between 2662°F and 2711 °F over 4.5 cycles. Each
cycle consisted of lowering the temperature continuously over 5 minutes and raising
the temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. At sweep count 0.5, a krypton radiation source was initiated in the sealed
enclosure. At sweep count 1.0, an argon radiation source was initiated in the sealed
enclosure. At sweep count 4.5, the short wave ultraviolet radiation source was terminated
in the sealed enclosure. The reactor temperature was lowered to 2645°F over 5 minutes.
The temperature was varied between 2467°F and 2645°F for 15.5 cycles. Each cycle consisted
of lowering the temperature continuously over 15 minutes and raising the temperature
continuously over 15 minutes. In addition, while raising the temperature, a 0.15 L/min
flow of 60% argon, 40% helium, and trace neon was added, and while lowering the temperature,
a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was added. After the
15.5
th cycle, third body gas addition was changed by turning off all gas components except
the trace neon gas flow.
[0105] After the 15.5
th cycle, a timer was established. At a time of 3 minutes, the xenon radiation source
within the sealed enclosure was remotely rotated. The timer was then reset to zero.
At 60 minutes, flow rates were adjusted to 0.3 L/min of 100% argon and trace neon.
At 65 minutes, flow rates were adjusted to 3.0 ml/min of 60% argon, 40% helium, and
trace neon. Immediately after the flow was adjusted, one of the neon radiation sources
within the sealed enclosure was remotely rotated. At 68 minutes, flow rates were adjusted
to 0.15 L/min of 100% helium, trace neon and trace krypton. At 68 minutes 20 seconds,
the 1 volt power was brought to zero output and the voltage power leads removed from
the voltage probes. At 68 minutes 30 seconds, the long wave ultraviolet radiation
source was turned off in the sealed enclosure. At 71 minutes 15 seconds, the voltage
probes were repositioned to three inches above the bath surface. At 75 minutes, the
source and ground probe were completely removed from the reactor.
[0106] After the voltage probes had been removed from the reactor, flow rates were adjusted
to 0.15 L/min of 77% argon, 18% nitrogen, 5% helium and trace neon. The reactor was
then held at temperature and flow rate for 15 minutes. After the 15 minute hold, an
argon radiation source was turned off in the sealed enclosure. The flow rates were
immediately readjusted to 0.15 L/min of 77% argon, 12% nitrogen, 11% helium and trace
neon. The reactor was then held at temperature and flow rate for 25 minutes. After
the 25 minute hold, the krypton radiation source was turned off in the sealed enclosure.
The flow rates were immediately readjusted to 0.30 L/min of 10% argon, 90% helium
and trace neon. The reactor was then held at temperature and flow rate for 3 minutes.
After the 3 minute hold, flow rates were adjusted to 0.15 L/min of 10% argon, 90%
helium and trace neon and held for 2 minutes. After the 2 minute hold, flow rates
were adjusted to 0.30 L/min of 7% hydrogen, 93% nitrogen and trace neon and held for
10 minutes. After the 10 minute hold, flow rates were adjusted to 0.15 L/min of 7%
hydrogen, 93% nitrogen and trace neon and held for 3 minutes. After the 3 minute hold,
flow rates were adjusted to 30 ml/min of 7% hydrogen, 93% nitrogen and trace neon
and held for 2 minutes. After the 2 minute hold, flow rates were adjusted to 0.15
L/min of 87% argon, 10% nitrogen, 3% helium and trace neon and held for 5 minutes.
After the 5 minute hold, flow rates were adjusted to 0.6 L/min of 90% argon, 10% nitrogen
and trace neon and held for 7 minutes. After the 7 minute hold, flow rates were adjusted
to 30 ml/min of 90% argon, 10% nitrogen and trace neon and held for 2 minutes. After
the 2 minute hold, flow rates were adjusted to 0.60 L/min of 95% argon, 5% nitrogen
and trace neon and held for 15 minutes. After the 15 minute hold, flow rates were
adjusted to 0.30 L/min of 95% argon, 5% nitrogen and trace neon and held for 5 minutes.
[0107] The reactor temperature was then lowered to 2541°F over 21 minutes. The temperature
was then varied between 2467°F and 2541°F for three cycles. The cycles consisted of
raising the temperature continuously over 27 minutes and lowering the temperature
continuously over 27 minutes. After the third cycle, the bath was held at 2541°F for
5 minutes. The reactor temperature was then lowered to 2467°F over 2 minutes 30 seconds.
The temperature was then varied between 2541°F and 2467°F for two cycles. The cycles
consisted of raising the temperature continuously over 11 minutes and lowering the
temperature continuously over 7 minutes.
[0108] After the completion of the 2
nd cycle, the induction power supply was placed into manual control. The power was then
instantaneously increased 5 kW above the steady state power level and immediately
upon hitting the 5kW increase the power was instantaneously decreased back to the
steady state power level. The power level was then varied up 3.7 kW and down 3.7 kW
over 6 cycles. The cycles consisted of raising power 3.7 kW above the steady state
power level over 25 seconds. Once raised, the power level was held at the additional
3.7 kW setting for 45 seconds. Following the 45 second hold, the power was lowered
back to the steady state power level over a 15 second time frame.
[0109] After the 6
th power cycle, the gas flows were adjusted to 0.60 L/min of 100% argon and trace neon
and held for 7 minutes. Following the seven minute hold, the argon flow was secured
leaving only the trace neon flow. Once the argon flow was secured, a second lance
was positioned inside the reactor. This lance was placed at a distance 2/3 from the
radial center and 1.5 inches from the bottom of the bath. The centerline lance was
then repositioned to ¼ inch from the bottom. Once the centerline lance was repositioned,
flow was started in the off-centerline lance at a rate of 30 ml/min of 100% argon
and trace neon. A timer was initiated. At a time of 2 minutes, the trace neon flow
in the centerline lance was secured. At a time of 2 minutes 30 seconds, flow was initiated
in the centerline lance at a flow rate of 30 ml/min of 100% carbon monoxide and held
for 3 minutes. After the 3 minute hold, flow rates were adjusted in the off-centerline
lance to 0.15 L/min of 100% argon and trace neon and held for 15 minutes. After the
15 minute hold, flow rates were adjusted in the off-centerline lance to trace neon
only. Furthermore, the flow rate was adjusted in the centerline lance to 0.60 L/min
of 100% carbon monoxide and held for 10 minutes. After the 10 minute hold, the carbon
monoxide in the centerline lance was secured. The reactor temperature was then lowered
to T
solidus plus 18°F over 30 minutes. Upon reaching the T
solidus plus 18°F, flow was adjusted in the centerline lance to 0.30 L/min of 100% carbon
monoxide and held for 20 minutes. After the 20 minute hold, all flow was secured in
the centerline lance and the lance was removed.
[0110] After the centerline lance was removed, adjust flow rates in the off-centerline lance
to 30 ml/min of 88% argon, 12% nitrogen and trace neon, and held for 3 minutes. After
the 3 minute hold, flow rates were adjusted to 0.30 L/min of 25% helium, 75% argon
and trace neon and held for 10 minutes. After the 10 minute hold, flow rates were
adjusted to 0.30 L/min of 88% argon, 12% nitrogen and trace neon and held for 10 minutes.
After the 10 minute hold, flow rates were adjusted to 0.15 L/min of 88% argon, 12%
nitrogen and trace neon and held for 5 minutes. After the 5 minute hold, flow rates
were adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon and held for
2 minutes. After the 2 minute hold, flow rates were adjusted to 0.15 L/min of 88%
argon, 12% nitrogen and trace neon. Once the flow rates were adjusted, the reactor
temperature was lowered to T
solidus plus 15°F over 45 minutes. Upon reaching the T
solidus plus 15°F, flow was adjusted in the off-centerline lance to 0.30 L/min of 100% argon
and trace neon and held for 5 minutes.
[0111] At the completion of the five minute hold, the reactor temperature was lowered to
T
solidus plus 11°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 11°F, adjust flow rate in the off-centerline lance to 0.30 L/min of 100% hydrogen
and trace neon. At the completion of flow adjustment, the reactor temperature was
lowered to T
solidus plus 10°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 10°F, adjust flow rate in the off-centerline lance to 30 ml/min of 100% hydrogen
and trace neon. At the completion of flow adjustment, the reactor temperature was
lowered to T
solidus plus 9°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 9°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch dimple (e.g., a quarter inch depression) could be observed
on the bath surface. The bath was held at T
solidus plus 9°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. Immediately after the 1.5 kW power pulse, flow was
adjusted in the off-centerline lance to 0.15 L/min of 50% hydrogen, 50% helium and
trace neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 75°F. Upon reaching T
solidus minus 75°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 60%
helium, 40% hydrogen and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.75 kW and the reactor was allowed to cool to
1000°F. Upon reaching 1000°F, flow rate in the off-centerline lance was adjusted to
30 ml/min of 100% helium and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.50 kW and the reactor was allowed to cool to
350°F. Upon reaching 350°F, the induction furnace power supply was shut down and a
timer initiated. At time of 5 minutes, flow rate in the off-centerline lance was adjusted
to 0.60 L/min of 100% helium and trace neon. At time of 9 minutes, a neon radiation
source within the sealed enclosure was remotely rotated. Upon completion of the rotation,
flow in the off-centerline lance was adjusted to 0.30 L/min of 88% argon, 12% nitrogen
and trace neon.
[0112] Following the flow adjustment, the timer was reinitiated. At a time of 25 seconds,
a neon radiation source within the sealed enclosure was remotely rotated. At a time
of 1 minute 30 seconds, a neon radiation source within the sealed enclosure was terminated.
At a time of 5 minutes an argon radiation source within the sealed enclosure was terminated.
At a time of 6 minute 30 seconds, flow rate was adjusted to 0.30 L/min of 100% helium
and trace neon. At a time of 7 minute, the second neon radiation source within the
sealed enclosure was terminated.
[0113] The timer was reset to zero and restarted. At a time of 15 minutes, the trace neon
gas flow in the off-centerline lance was terminated. At a time of 17 minutes 25 seconds,
the xenon radiation source within the sealed enclosure was remotely rotated. At a
time of 30 minutes, the trace helium gas flow in the off-centerline lance was terminated.
The timer was reset to zero and restarted. At a time of 15 minutes, the xenon radiation
source inside the sealed enclosure was terminated. Thirty minutes were allowed to
pass. The ingot and crucible were removed from the reactor in the presence of radiation
sources (metal halide light sources) utilizing titanium metal tongs.
[0114] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches of DI water. Upon entrance into the quench chamber, a timer was
established. At a time of 2 hours 15 minutes, a long wave ultraviolet radiation source
located above the quench vessel was initiated. At a time of 4 hours 7 minutes, a short
wave ultraviolet radiation source located above the quench vessel was initiated. At
a time of 5 hours 59 minutes 30 seconds the short wave ultraviolet radiation source
located above the quench vessel was rotated to a tip up position.
[0115] At a time of 6 hours, the ingot was removed from the quench system using the titanium
metal tongs and transferred to a clean radiation surface countertop. Exposure to external
radiation sources included the metal halide light and placement directly under a skylight
(which added filtered sunlight to the irradiation sources). The ingot was pat dried.
Upon completion of the drying, the long wave ultraviolet radiation source located
above the quench vessel was rotated vertically and moved up 1 inch. The timer was
then reset to zero. The ingot was irradiated for 10 minutes at which point an additional
radiation source (krypton lamp) was initiated. At 12 minutes 30 seconds, the long
wave ultraviolet radiation source located above the quench vessel was rotated to horizontal
and moved down to its original position. At 13 minutes, a xenon radiation source located
above the quench vessel was initiated. At 18 minutes, two orthogonal fluorescent lamp
racks located next to the countertop were turned on. At 30 minutes, two angled metal
halide lights located next to the countertop were simultaneously turned on. At this
point the timer was again reset. At 13 minutes 15 seconds, a neon radiation source
located next to the countertop was turned on. At 15 minutes 30 seconds, an argon radiation
source located next to the countertop was turned on. At 23 minutes 45 seconds, the
argon radiation source located next to the countertop was rotated to an angle of 35°.
At 37 minutes 30 seconds the short wave ultraviolet radiation source located above
the quench vessel was rotated to 35°. At 47 minutes 30 seconds, the xenon radiation
source located above the quench vessel was rotated to horizontal. At 52 minutes 45
seconds, the long wave ultraviolet radiation source located above the quench vessel
was rotated to 35°. At 58 minutes 30 seconds, the short wave ultraviolet radiation
source located above the quench vessel was rotated to 55°. At 77 minutes, the krypton
radiation source located next to the countertop was rotated to vertical. At 89 minutes,
the krypton radiation source located next to the countertop was rotated to 78°. At
97 minutes, the krypton radiation source located next to the countertop was rotated
to 88°.
[0116] At this point the timer was again reset. At a time of 6 hours, the krypton lamp,
short wave ultraviolet, long wave ultraviolet, argon (located over quench vessel),
xenon, argon (located next to countertop), neon, two orthogonal fluorescent lamp racks,
and the two angled metal halide lights were sequentially terminated in the given order.
The timer was again reset. At a time of 6 hours, 30 minutes, normal lab lighting (metal
halides) was turned off. The timer was reset. For 48 hours, the ingot was allowed
to stabilize with no manual intervention (i.e., no handling).
EXAMPLE 5:
EXPERIMENTAL PROCEDURE FOR NICKEL, RHENIUM Method "HD" RUN 14-01-21
[0117] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08%Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100-pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply. A gas
addition lance was installed to a position approximately ¼ inches from the bottom
of the reactor. The reactor was charged with 9080 g nickel (99.9% purity) and 5 g
rhenium (99.997% purity) through its charging port. The reactor was fitted with a
graphite cap and a ceramic liner (i.e., the crucible, from Engineering Ceramics).
During the entire procedure, a slight positive pressure of 97% argon, 3% hydrogen
(~0.5 psig) was maintained in the reactor using a continuous backspace purge. Bypass
injection of gas addition was commenced (i.e., gas flow diverted around the reactor
was initiated) at a rate of 0.15 L/min of argon. The incoming gas line for the gas
addition lance passed through a sealed, light-tight enclosure whereby irradiation
of the gas with precise radiation sources (e.g., wavelength, intensity, etc) was achieved.
When the entire gas line had been completely purged (assuming a plug flow model),
a neon radiation source was activated within the sealed enclosure. A timer was initiated.
Bypass flow was adjusted to 100% argon at a flow rate of 0.15 L/min with trace neon
present (trace can be defined as ≤ 0.005% vol. to ≤ 5%). At a time of 3 minutes, an
argon radiation source was activated within the sealed enclosure. After completion
of another gas line purge (assuming a plug flow model), the gas line was switched
from bypass to direct injection through the gas addition lance.
[0118] The induction furnace power was then initiated. The reactor was heated to 450°F,
at a rate no greater than 300°F/hr, as limited by the integrity of the crucible. The
induction furnace operated in the frequency range of 0 Hz to 3000 Hz, with frequency
determined by a temperature-controlled feedback loop implementing an Omega Model CN3000
temperature controller. Upon reaching 450°F, the gas addition lance was repositioned
to 2 inches from the bottom of the reactor. The timer was reinitiated. At a time of
2 minutes, the gas composition was changed to 0.15 L/min of 66% nitrogen, 34% hydrogen
and trace neon. After completion of another gas line purge (assuming a plug flow model),
a krypton radiation source was initiated in the sealed enclosure. The reactor continued
to heat up at a rate no greater than 300°F/hr, as limited by the integrity of the
crucible, until T
solidus minus 30°F was achieved. The gas flow rate was then increased to 0.3 L/min with a
constant gas composition. At T
solidus a second argon radiation source was activated within the sealed enclosure. Approach
T
solidus plus 8°F over a 3 to 5 minute time span. From T
solidus plus 8°F to T
solidus plus 15°F, reduce the gas flow rate to 0.15 L/min with a constant gas composition.
Immediately upon reaching T
solidus plus 15°F, a second neon radiation source was initiated in the sealed enclosure.
Immediately after the second neon radiation source was initiated, the gas composition
was adjusted to 75% hydrogen, 22% nitrogen, 3% argon, and trace neon. The molten bath
was held at this condition for 5 minutes for stabilization.
[0119] After the 5-minute hold, the gas composition was adjusted to 20% helium, 63% nitrogen,
17% argon, and trace neon. The bath was held under these conditions for an additional
15 minutes. Again, following the hold, the gas composition and flow rate were adjusted
to 100% argon with trace neon at a rate of 0.3 L/min. The reactor was held at this
condition for 3 minutes. The timer was reinitiated. At a time of 65 minutes, graphite
saturation assemblies (3/8 inches OD, 36 inches long high purity (<5 ppm impurities)
graphite rods) were inserted to the bottom of the nickel alloy charge through ports
located in the top plate. The nickel was heated to 2540°F over a one-hour period.
The bath was then held at this condition for 2 hours. Every 30 minutes during the
hold period, an attempt was made to lower the graphite saturation assemblies as dissolution
occurred. As the nickel became saturated with carbon, the graphite saturation assemblies
were consumed. After the 2-hour hold period was complete, the graphite saturation
assemblies were removed. An additional 40 grams of graphite powder was charged into
the reactor through the charging port. The bath was then heated to 3390°F over three
hours. Upon achieving 3390°F, the gas composition and flow rate were adjusted to 100%
nitrogen with trace neon at a rate of 0.3 L/min. The reactor conditions were held
for 5 minutes and the gas flow rate was reduced to 0.15L/min with constant composition.
Immediately following this reduction in gas flow, the krypton radiation source in
the sealed enclosure was turned off. The timer was reinitiated. At a time of 3 minutes,
the gas flow rate was reduced to 37.5 ml/min with constant composition. One of the
argon radiation sources inside the sealed enclosure was turned off. At a time of 5
minutes, the nitrogen component of the gas flow was discontinued, while maintaining
the flow of the trace neon. At a time of 10 minutes, one of the neon radiation sources
within the sealed enclosure was remotely rotated. The reactor temperature was lowered
to 3193°F over 7 minutes.
[0120] The temperature was then varied between 2897°F and 3193°F for 16 cycles. Each cycle
consisted of raising the temperature continuously over 7 minutes and lowering the
temperature continuously over 7 minutes. After completion of the 14.5 cycles, argon
is reintroduced at a flow rate of 0.15 L/min with trace neon. Five minutes into the
15
th cycle, a xenon radiation source was activated within the sealed enclosure. At 6 minutes
into the 15
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, a short wave ultraviolet radiation source was initiated in the
sealed enclosure. At sweep count 16, remotely rotate the xenon radiation source within
the sealed enclosure. The temperature of the nickel was varied over another 5 cycles
between 2897°F and 3193°F. After the fifth cycle, the reactor temperature was lowered
to 2800°F over a 60-minute period. Upon achieving the target temperature of 2800°F,
the graphite saturation assemblies were reinstalled in the nickel and remained there
for 1 hour. The graphite saturation assemblies were then removed.
[0121] Two voltage probes (source and ground probe) were then installed in the headspace
of the reactor and allowed to equilibrate for 5 minutes. Upon completion of the five-minute
hold, the voltage probes are lowered into the bath. The source probe was positioned
2 inches below the axial center and 1 inch from the radial center. The ground probe
was positioned 0.75 inches above the axial position of the source probe and 1 inch
from the radial center (180° from the source probe). Once the probes were installed,
a five-minute hold at this condition was done to allow the bath to electronically
equilibrate with the probes. Voltage was then applied to the probes and varied between
multiple voltage set points. This voltage was in a continuous up/down sweep between
two predetermined voltages. The first voltage cycle was varied between 17 and 18 volts
for 24 cycles. Each cycle consisted of raising the voltage continuously over 45 seconds
and lowering the voltage continuously over 45 seconds. The second voltage cycle was
varied between 13.25 and 14.75 volts for 20 cycles. Each cycle consisted of raising
the voltage continuously over 45 seconds and lowering the voltage continuously over
45 seconds. The third voltage cycle was varied between 8.75 and 10.25 volts for 17
cycles. Each cycle consisted of raising the voltage continuously over 45 seconds and
lowering the voltage continuously over 45 seconds. The fourth voltage cycle was varied
between 4.00 and 7.00 volts for 14 cycles. Each cycle consisted of raising the voltage
continuously over 45 seconds and lowering the voltage continuously over 45 seconds.
The fifth voltage cycle was varied between 1.50 and 5.00 volts for 10 cycles. Each
cycle consisted of raising the voltage continuously over 45 seconds and lowering the
voltage continuously over 45 seconds. The sixth voltage cycle was varied between 0.50
and 2.00 volts for 3 cycles. Each cycle consisted of raising the voltage continuously
over 45 seconds and lowering the voltage continuously over 45 seconds. When the final
cycle was completed the voltage was set onto a constant 1-volt setting. This voltage
remained constant until a later step during which the leads were removed.
[0122] The reactor temperature was then lowered to 2780°F over 5 minutes. The reactor was
held at this temperature for 5 minutes with continued gas addition. The temperature
was then varied between 2741°F and 2780°F over 20 cycles. Each cycle consisted of
lowering the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. After the 20
th cycle, turning off the argon component of the gas leaving only traces of neon gas
flow changed third body gas addition. The bath was then cooled to 2722°F over 5 minutes.
Upon reaching 2722°F, one of the neon radiation sources within the sealed enclosure
was remotely rotated.
[0123] The temperature was then varied between 2664°F and 2722°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. At sweep count 0.5, a krypton radiation source was initiated in the sealed
enclosure. At sweep count 1.0, an argon radiation source was initiated in the sealed
enclosure. At sweep count 4.5, a short wave ultraviolet radiation source was terminated
in the sealed enclosure. The reactor temperature was lowered to 2645°F over 5 minutes.
The temperature was varied between 2451°F and 2645°F for 15.5 cycles. Each cycle consisted
of lowering the temperature continuously over 15 minutes and raising the temperature
continuously over 15 minutes. In addition, while raising the temperature, a 0.15 L/min
flow of 60% argon, 40% helium, and trace neon was added, and while lowering the temperature,
a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was added. After the
15.5
th cycle, turning off all gas components except the trace neon gas flow changed third
body gas addition.
[0124] After the 15.5
th cycle, a timer was initiated. At a time of 3 minutes, the xenon radiation source
within the sealed enclosure was remotely rotated. The timer was reinitiated. At 60
minutes, flow rates were adjusted to 0.3 L/min of 100% argon and trace neon. At 65
minutes, flow rates were adjusted to 3.0 ml/min of 60% argon, 40% helium, and trace
neon. Immediately after the flow was adjusted, remotely rotate one of the neon radiation
sources within the sealed enclosure. At 68 minutes, flow rates were adjusted to 0.15
L/min of 100% helium, trace neon and trace krypton. At 68 minutes 20 seconds, the
1-volt power was brought to zero output and the voltage power leads removed from the
voltage probes. At 68 minutes 30 seconds, the long wave ultraviolet radiation source
was turned off in the sealed enclosure. At 71 minutes 15 seconds, reposition the voltage
probes to three inches above the bath surface. At 75 minutes, remove the source and
ground probes completely from the reactor.
[0125] After the voltage probes had been removed from the reactor, flow rates were adjusted
to 0.15 L/min of 77% argon, 18% nitrogen, 5% helium, and trace neon. The reactor was
then held at temperature and flow rate for 15 minutes. After the 15-minute hold, an
argon radiation source was turned off in the sealed enclosure. The flow rates were
immediately readjusted to the flow rate 0.15 L/min of 77% argon, 12% nitrogen, 11
% helium, and trace neon. The reactor was then held at temperature and flow rate for
25 minutes. After the 25-minute hold, the krypton radiation source was turned off
in the sealed enclosure. The flow rates were immediately readjusted to the flow rate
0.30 L/min of 10% argon, 90% helium and trace neon. The reactor was then held at temperature
and flow rate for 3 minutes. After the 3-minute hold, flow rates were adjusted to
0.15 L/min of 10% argon, 90% helium and trace neon and held for 2 minutes. After the
2-minute hold, flow rates were adjusted to 0.30 L/min of 7% hydrogen, 93% nitrogen
and trace neon and held for 10 minutes. After the 10-minute hold, flow rates were
adjusted to the flow rate of 0.15 L/min of 7% hydrogen, 93% nitrogen and trace neon
and held for 3 minutes. After the 3-minute hold, flow rates were adjusted to 30 ml/min
of 7% hydrogen, 93% nitrogen and trace neon and held for 2 minutes. After the 2-minute
hold, flow rates were adjusted to 0.15 L/min of 87% argon, 10% nitrogen, 3% helium,
and trace neon and held for 5 minutes. After the 5-minute hold, flow rates were adjusted
to 0.6 L/min of 90% argon, 10% nitrogen and trace neon and held for 7 minutes. After
the 7-minute hold, flow rates were adjusted to 30 ml/min of 90% argon, 10% nitrogen
and trace neon and held for 2 minutes. After the 2-minute hold, flow rates were adjusted
to 0.60 L/min of 95% argon, 5% nitrogen and trace neon and held for 15 minutes. After
the 15-minute hold, flow rates were adjusted to 0.30 L/min of 95% argon, 5% nitrogen
and trace neon and held for 5 minutes.
[0126] The reactor temperature was lowered to 2529°F over 21 minutes. The temperature was
then varied between 2451 °F and 2529°F for three cycles. The cycle consisted of raising
the temperature continuously over 27 minutes and lowering the temperature continuously
over 27 minutes. After the third cycle, the bath was held at 2529°F for 5 minutes.
The reactor temperature was then lowered to 2451°F over 2 minutes 30 seconds. The
temperature was then varied between 2529°F and 2451°F for two cycles. The cycles consisted
of raising the temperature continuously over 11 minutes and lowering the temperature
continuously over 7 minutes.
[0127] After completion of the 2
nd cycle, the induction power supply was placed into manual control. The power was then
instantaneously increased 5 kW above the steady state power level and immediately
upon hitting the 5 kW increase the power was instantaneously decreased back to the
steady state power level. The power level was then varied up 3.7 kW and down 3.7 kW
over 6 cycles. The cycles consisted of raising power 3.7 kW above the steady state
power level over 25 seconds. Once raised, the power level was held at the additional
3.7 kW setting for 45 seconds. Following the 45 second hold, the power was lowered
back to the steady state power level over a 15 second time frame.
[0128] After the 6
th power cycle, the gas flows were adjusted to 0.60 L/min of 100% argon and trace neon
and held for 7 minutes. Following the seven-minute hold, the argon flow was secured
leaving only the trace neon flow. Once the argon flow was secured, a second lance
was positioned inside the reactor. This lance was placed at a distance 2/3 from the
radial center and 1.5 inches from the bottom of the bath. The centerline lance was
then repositioned to ¼ inch from the bottom. Once the centerline lance was repositioned,
flow was started in the off-centerline lance at a rate of 30 ml/min of 100% argon
and trace neon. A timer was reinitiated. At a time of 2 minutes, the trace neon flow
in the centerline lance was secured. At a time of 2 minutes 30 seconds, flow was initiated
in the centerline lance at a flow rate of 30 ml/min of 100% carbon monoxide and held
for 3 minutes. After the 3-minute hold, flow rates were adjusted in the off-centerline
lance to 0.15 L/min of 100% argon and trace neon and held for 15 minutes. After the
15-minute hold, flow rates were adjusted in the off-centerline lance to trace neon
only. Furthermore, the flow rate was adjusted in the centerline lance to 0.60 L/min
of 100% carbon monoxide and held for 10 minutes. After the 10-minute hold, the carbon
monoxide in the centerline lance was secured. The reactor temperature was then lowered
to T
solidus plus 18°F over 30 minutes. Upon reaching the T
solidus plus 18°F, flow was adjusted in the centerline lance to 0.30 L/min of 100% carbon
monoxide and held for 20 minutes. After the 20-minute hold, all flow was secured in
the centerline lance and the lance was removed.
[0129] After the centerline lance was removed, flow rates in the off-centerline lance were
adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon, and held for 3 minutes.
After the 3-minute hold, flow rates were adjusted to 0.30 L/min of 25% helium, 75%
argon and trace neon and held for 10 minutes. After the 10-minute hold, flow rates
were adjusted to 0.30 L/min of 88% argon, 12% nitrogen and trace neon and held for
10 minutes. After the 10-minute hold, flow rates were adjusted to 0.15 L/min of 88%
argon, 12% nitrogen and trace neon and held for 5 minutes. After the 5-minute hold,
flow rates were adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon and
held for 2 minutes. After the 2-minute hold, flow rates were adjusted to 0.15 L/min
of 88% argon, 12% nitrogen and trace neon. Once the flow rate was adjusted, the reactor
temperature was lowered to T
solidus plus 15°F over 45 minutes. Upon reaching the T
solidus plus 15°F, flow was adjusted in the off-centerline lance to 0.30 L/min of 100% argon
and trace neon and held for 5 minutes.
[0130] At the completion of the five minute hold, the reactor temperature was lowered to
T
solidus plus 11°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 11°F, flow rate in the off-centerline lance was adjusted to 0.30 L/min of 100%
hydrogen and trace neon. At the completion of flow adjustment, the reactor temperature
was lowered to T
solidus plus 10°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 10°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 100%
hydrogen and trace neon. At the completion of the flow adjustment, the reactor temperature
was lowered to T
solidus plus 9°F while maintaining a temperature-lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 9°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch (1/4 inches) dimple could be observed on the bath surface.
The bath was held at T
solidus plus 9°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. Immediately after the 1.5 kW power pulse, flow was
adjusted in the off-centerline lance to 0.15 L/min of 50% hydrogen, 50% helium and
trace neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 75°F. Upon reaching T
solidus minus 75°F, adjust flow rate in the off-centerline lance to 30 ml/min of 60% helium,
40% hydrogen and trace neon. Following the flow adjustment, the induction furnace
power supply was lowered to 0.75 kW and the reactor was allowed to cool to 1000°F.
Upon reaching 1000°F, flow rate in the off-centerline lance was adjusted to 30 ml/min
of 100% helium and trace neon. Following the flow adjustment, the induction furnace
power supply was lowered to 0.50 kW and the reactor was allowed to cool to 350°F.
Upon reaching 350°F, the induction furnace power supply was shut down and a timer
initiated. At a time of 5 minutes, flow rate in the off-centerline lance was adjusted
to 0.60 L/min of 100% helium and trace neon. At a time of 9 minutes, a neon radiation
source within the sealed enclosure was remotely rotated. Upon completion of the rotation,
flow in the off-centerline lance was adjusted to 0.30 L/min of 88% argon, 12% nitrogen
and trace neon.
[0131] Following the flow adjustment, the timer was reinitiated. At a time of 25 seconds,
a neon radiation source within the sealed enclosure was remotely rotated. At a time
of 1 minute 30 seconds, a neon radiation source within the sealed enclosure was terminated.
At a time of 5 minutes, an argon radiation source within the sealed enclosure was
terminated. At a time of 6 minutes 30 seconds, flow rate was adjusted to 0.30 L/min
of 100% helium and trace neon. At a time of 7 minute, the second neon radiation source
within the sealed enclosure was terminated.
[0132] The timer was reinitiated. At a time of 15 minutes, the trace neon gas flow in the
off-centerline lance was terminated. At a time of 17 minutes 25 seconds, the xenon
radiation source within the sealed enclosure was remotely rotated. At a time of 30
minutes, the trace helium gas flow in the off-centerline lance was terminated. The
timer was reinitiated. At a time of 15 minutes, the xenon radiation source inside
the sealed enclosure was terminated. Thirty minutes were allowed to pass. The ingot
and crucible were removed from the reactor in the presence of radiation sources (metal
halide light sources) utilizing titanium metal tongs.
[0133] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches ofDI water. Upon entrance into the quench chamber, a timer was
established. At a time of 2 hours 15 minutes, a long wave ultraviolet radiation source
located above the quench vessel was initiated. At a time of 4 hours 7 minutes, a short
wave ultraviolet radiation source located above the quench vessel was initiated. At
a time of 5 hours 59 minutes 30 seconds, the short wave ultraviolet radiation source
located above the quench vessel was rotated to a vertical position.
[0134] At a time of 6 hours, the ingot was removed from the quench system using the titanium
metal tongs and transferred to a clean radiation surface countertop. Exposure to external
radiation sources included the metal halide light and placement directly under a skylight
(which added filtered sunlight to the irradiation sources). The ingot was pat dried.
Upon completion of the drying, the long wave ultraviolet radiation source located
above the quench vessel was rotated vertical and moved up 1 inch. The timer was then
reinitiated. The ingot was irradiated for 10 minutes at which point an additional
radiation source (krypton lamp) was initiated. At 12 minutes 30 seconds, the long
wave ultraviolet radiation source located above the quench vessel was rotated horizontal
and moved down to its original position. At 13 minutes, a xenon radiation source located
above the quench vessel was initiated. At 18 minutes, two orthogonal fluorescent lamp
racks located next to the countertop were turned on. At 30 minutes, two angled metal
halide lights located next to the countertop were simultaneously turned on. At this
point the timer was again reinitiated. At 13 minutes 15 seconds, a neon radiation
source located next to the countertop was turned on. At 15 minutes 30 seconds, an
argon radiation source located next to the countertop was turned on. At 23 minutes
45 seconds, the argon radiation source located next to the countertop was rotated
to an angle of 35°. At 37 minutes 30 seconds, the short wave ultraviolet radiation
source located above the quench vessel was rotated to 35°. At 47 minutes 30 seconds,
the xenon radiation source located above the quench vessel was rotated to horizontal.
At 52 minutes 45 seconds, the long wave ultraviolet radiation source located above
the quench vessel was rotated to 35°. At 58 minutes 30 seconds, the short wave ultraviolet
radiation source located above the quench vessel was rotated to 55°. At 77 minutes,
the krypton radiation source located next to the countertop was rotated to vertical.
At 89 minutes, the krypton radiation source located next tot eh countertop was rotated
78°. At 93 minutes, the ingot was lifted using composite black rubber gloves and a
tailored material that acts as an energy filter was placed under the ingot. The tailored
material used as an energy filter has an XRF as depicted in the Appendix 1. The ingot
was then lowered onto the tailored energy filter.
[0135] At this point the timer was again reset. At a time of 6 hours, the krypton lamp,
short wave ultraviolet, long wave ultraviolet, argon (located over quench vessel),
xenon, argon (located next to countertop), neon, two orthogonal fluorescent lamp racks,
and the two angled metal halide lights were sequentially terminated in the given order.
The timer was again reset. At a time of 6 hours, 30 minutes, normal lab lighting (metal
halides) was turned off. The timer was reset. For 48 hours, the ingot was allowed
to stabilize with no manual intervention (i.e., no handling).
EXAMPLE 6:
EXPERIMENTAL PROCEDURE FOR IRON, VANADIUM, CHROMIUM, MANGANESE Method "HD" RUN 14-01-13
[0136] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100-pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply. A gas
addition lance was installed to a position approximately ¼ inches from the bottom
of the reactor. The reactor was charged with 8534 g iron (99.98% purity), 182 g vanadium
(99.5% purity), 182 g chromium (99.999% purity) and 182 g manganese (99.99% purity)
through its charging port. The reactor was fitted with a graphite cap and a ceramic
liner (i.e., the crucible, from Engineering Ceramics). During the entire procedure,
a slight positive pressure of 97% argon, 3% hydrogen (~0.5 psig) was maintained in
the reactor using a continuous backspace purge. Bypass injection of gas addition was
commenced (i.e., gas flow diverted around the reactor was initiated) at a rate of
0.15 L/min of argon. The incoming gas line for the gas addition lance passed through
a sealed, light-tight enclosure whereby irradiation of the gas with precise radiation
sources (e.g., wavelength, intensity, etc) was achieved. When the entire gas line
had been completely purged (assuming a plug flow model), a neon radiation source was
activated within the sealed enclosure. A timer was initiated. Bypass flow was adjusted
to 100% argon at a flow rate of 0.15 L/min with trace neon present (trace can be defined
as ≤ 0.005% volume to ≤ 5%). At a time of 3 minutes, an argon radiation source was
activated within the sealed enclosure. After completion of another gas line purge
(assuming a plug flow model), the gas line was switched from bypass to direct injection
through the gas addition lance.
[0137] The induction furnace power was then initiated. The reactor was heated to 450°F,
at a rate no greater than 300°F/hr, as limited by the integrity of the crucible. The
induction furnace operated in the frequency range of 0 Hz to 3000 Hz, with frequency
determined by a temperature-controlled feedback loop implementing an Omega Model CN3000
temperature controller. Upon reaching 450°F, the gas addition lance was repositioned
to 2 inches from the bottom of the reactor. The timer was reinitiated. At a time of
2 minutes, the gas composition was changed to 0.15 L/min of 66% nitrogen, 34% hydrogen
and trace neon. After completion of another gas line purge (assuming a plug flow model),
a krypton radiation source was initiated in the sealed enclosure. The reactor heat
up continued at a rate no greater than 300°F/hr, as limited by the integrity of the
crucible, until T
solidus minus 30°F was achieved. The gas flow rate was then increased to 0.3 L/min with a
constant gas composition. At T
solidus a second argon radiation source was activated within the sealed enclosure. Approach
T
solidus plus 8°F over a 3 to 5 minute time span. From T
solidus plus 8°F to T
solidus plus 15°F, reduce the gas flow rate to 0.15 L/min with a constant gas composition.
Immediately upon reaching T
solidus plus 15°F, a second neon radiation source was initiated in the sealed enclosure.
Immediately after the second neon radiation source was initiated, the gas composition
was adjusted to 75% hydrogen, 22% nitrogen, 3% argon, and trace neon. The molten bath
was held at this condition for 5 minute for stabilization.
[0138] After the 5-minute hold, the gas composition was adjusted to 20% helium, 63% nitrogen,
17% argon, and trace neon. The bath was held under these conditions for an additional
15 minutes. Again, following the hold, the gas composition and flow rate were adjusted
to 100% argon with trace neon at a rate of 0.3 L/min. The reactor was held at this
condition for 3 minutes. The timer was reinitiated. At a time of 65 minutes, graphite
saturation assemblies (3/8 inches OD, 36 inches long high purity (<5 ppm impurities)
graphite rods) were inserted to the bottom of the iron alloy charge through ports
located in the top plate. The iron was cooled to 2243°F over a two-hour period. The
bath was cooled due to the t-solidus temperature of an iron bath with no carbon versus
the temperature requirement of a carbon-containing bath. The bath was then held at
this condition for 2 hours. Every 30 minutes during the hold period, an attempt was
made to lower the graphite saturation assemblies as dissolution occurred. As the iron
alloy became saturated with carbon, the graphite saturation assemblies were consumed.
After the 2-hour hold period was complete, the graphite saturation assemblies were
removed. An additional 90 grams of graphite powder was charged into the reactor through
the charging port. The bath was then heated to 3525°F over three hours. Upon achieving
3525°F, the gas composition and flow rate were adjusted to 100% nitrogen with trace
neon at a rate of 0.3 L/min and held for 5 minutes. Reduce the gas flow rate to 0.15
L/min with constant composition. Immediately following this reduction in gas flow,
the krypton radiation source in the sealed enclosure was turned off. The timer was
reinitiated. At a time of 3 minutes, the gas flow rate was reduced to 37.5 ml/min
with constant composition. One of the argon radiation sources inside the sealed enclosure
was turned off. At a time of 5 minutes, the nitrogen component of the gas flow was
discontinued while maintaining the flow of the trace neon. At a time of 10 minutes,
one of the neon radiation sources within the sealed enclosure was remotely rotated.
The reactor temperature was lowered to 3360°F over 7 minutes.
[0139] The temperature was then varied between 2993°F and 3360°F for 16 cycles. Each cycle
consisted of raising the temperature continuously over 7 minutes and lowering the
temperature continuously over 7 minutes. After completion of the 14.5 cycles, argon
was reintroduced at a flow rate of 0.15 L/min with trace neon. Five minutes into the
15
th cycle, a xenon radiation source was activated within the sealed enclosure. At 6 minutes
into the 15
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, a short wave ultraviolet radiation source was initiated in the
sealed enclosure. At sweep count 16, the xenon radiation source within the sealed
enclosure was remotely rotated. The temperature of the iron alloy was varied over
another 5 cycles between 2993°F and 3360°F. After the fifth cycle, the reactor temperature
was then lowered to 2850°F over a 60-minute period. Upon achieving the target temperature
of 2850, the graphite saturation assemblies were reinstalled in the iron alloy and
remained there for 1 hour. The graphite saturation assemblies were then removed.
[0140] Two voltage probes (source and ground probe) were then installed in the headspace
of the reactor and allowed to equilibrate for 5 minutes. Upon completion of the five-minute
hold the voltage probes were lowered into the bath. The source probe was positioned
2 inches below the axial center and 1 inch from the radial center. The ground probe
was positioned 0.75 inches above the axial position of the source probe and 1 inch
from the radial center (180° from the source probe). Once the probes were installed
a five-minute hold at this condition was done to allow the bath to electronically
equilibrate with the probes. Voltage was then applied to the probes and varied between
multiple voltage set points. This voltage was in a continuous up/down sweep between
two predetermined voltages. The first voltage cycle was varied between 17 and 18 volts
for 24 cycles. Each cycle consisted of raising the voltage continuously over 45 seconds
and lowering the voltage continuously over 45 seconds. The second voltage cycle was
varied between 13.25 and 14.75 volts for 20 cycles. Each cycle consisted of raising
the voltage continuously over 45 seconds and lowering the voltage continuously over
45 seconds. The third voltage cycle was varied between 8.75 and 10.25 volts for 17
cycles. Each cycle consisted of raising the voltage continuously over 45 seconds and
lowering the voltage continuously over 45 seconds. The fourth voltage cycle was varied
between 4.00 and 7.00 volts for 14 cycles. Each cycle consisted of raising the voltage
continuously over 45 seconds and lowering the voltage continuously over 45 seconds.
The fifth voltage cycle was varied between 1.50 and 5.00 volts for 10 cycles. Each
cycle consisted of raising the voltage continuously over 45 seconds and lowering the
voltage continuously over 45 seconds. The sixth voltage cycle was varied between 0.50
and 2.00 volts for 3 cycles. Each cycle consisted of raising the voltage continuously
over 45 seconds and lowering the voltage continuously over 45 seconds. When the final
cycle was completed the voltage was set onto a constant 1-volt setting. This voltage
remains constant until a later step when the leads are removed.
[0141] The reactor temperature was lowered to 2819°F over 5 minutes. The reactor was held
at this temperature for 5 minutes with continued gas addition. The temperature was
then varied between 2757°F and 2819°F over 20 cycles. Each cycle consisted of lowering
the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. After the 20
th cycle, turning off the argon component of the gas leaving only trace neon gas flow
changed third body gas addition. The bath was then cooled to 2724°F over 5 minutes.
Upon reaching 2724°F, one of the neon radiation sources within the sealed enclosure
was remotely rotated.
[0142] The temperature was then varied between 2622°F and 2724°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. At sweep count 0.5, a krypton radiation source was initiated in the sealed
enclosure. At sweep count 1.0, an argon radiation source was initiated in the sealed
enclosure. At sweep count 4.5, a short wave ultraviolet radiation source was terminated
in the sealed enclosure. The reactor temperature was lowered to 2586°F over 5 minutes.
The temperature was varied between 2133°F and 2586°F for 15.5 cycles. Each cycle consisted
of lowering the temperature continuously over 15 minutes and raising the temperature
continuously over 15 minutes. In addition, while raising the temperature, a 0.15 L/min
flow of 60% argon, 40% helium, and trace neon was added, and while lowering the temperature,
a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was added. After the
15.5
th cycle, turning off all gas components except the trace neon gas flow changed third
body gas addition.
[0143] After the 15.5
th cycle, a timer was initiated. At a time of 3 minutes, remotely rotate the xenon radiation
source within the sealed enclosure. The timer was then reinitiated. At 60 minutes,
flow rates were adjusted to 0.3 L/min of 100% argon and trace neon. At 65 minutes,
flow rates were adjusted to 30 ml/min of 60% argon, 40% helium, and trace neon. Immediately
after the flow was adjusted, one of the neon radiation sources within the sealed enclosure
was remotely rotated. At 68 minutes, flow rates were adjusted to 0.15 L/min of 100%
helium, trace neon and trace krypton. At 68 minutes 20 seconds, the 1-volt power was
brought to zero output and the voltage power leads removed from the voltage probes.
At 68 minutes 30 seconds, the long wave ultraviolet radiation source was turned off
in the sealed enclosure. At 71 minutes 15 seconds, the voltage probes were repositioned
to three inches above the bath surface. At 75 minutes, the source and ground probe
were removed completely from the reactor.
[0144] After the voltage probes had been removed from the reactor, flow rates were adjusted
to 0.15 L/min of 77% argon, 18% nitrogen, 5% helium, and trace neon. The reactor was
then held at temperature and flow rate for 15 minutes. After the 15-minute hold, an
argon radiation source was turned off in the sealed enclosure. The flow rates were
immediately readjusted to the flow rate 0.15 L/min of 77% argon, 12% nitrogen, 11%
helium, and trace neon. The reactor was then held at temperature and flow rate for
25 minutes. After the 25-minute hold, the krypton radiation source was turned off
in the sealed enclosure. The flow rates were immediately readjusted to a flow rate
of 0.30 L/min of 10% argon, 90% helium and trace neon. The reactor was then held at
temperature and flow rate for 3 minutes. After the 3-minute hold, flow rates were
adjusted to 0.15 L/min of 10% argon, 90% helium and trace neon and held for 2 minutes.
After the 2-minute hold, flow rates were adjusted to 0.30 L/min of 7% hydrogen, 93%
nitrogen and trace neon and held for 10 minutes. After the 10-minute hold, flow rates
were adjusted to 0.15 L/min of 7% hydrogen, 93% nitrogen and trace neon and held for
3 minutes. After the 3-minute hold, flow rates were adjusted to 30 ml/min of 7% hydrogen,
93% nitrogen and trace neon and held for 2 minutes. After the 2-minute hold, flow
rates were adjusted to 0.15 L/min of 87% argon, 10% nitrogen, 3% helium, and trace
neon and held for 5 minutes. After the 5-minute hold, flow rates were adjusted to
0.6 L/min of 90% argon, 10% nitrogen and trace neon and held for 7 minutes. After
the 7-minute hold, flow rates were adjusted to 30 ml/min of 90% argon, 10% nitrogen
and trace neon and held for 2 minutes. After the 2-minute hold, flow rates were adjusted
to 0.60 L/min of 95% argon, 5% nitrogen and trace neon and held for 15 minutes. After
the 15-minute hold, flow rates were adjusted to 0.30 L/min of 95% argon, 5% nitrogen
and trace neon and held for 5 minutes.
[0145] The reactor temperature was raised to 2340°F over 21 minutes. The temperature was
then varied between 2133°F and 2340°F for three cycles. The cycle consisted of raising
the temperature continuously over 27 minutes and lowering the temperature continuously
over 27 minutes. After the third cycle, the bath was held at 2340°F for 5 minutes.
The reactor temperature was then lowered to 2133°F over 2 minutes 30 seconds. The
temperature was then varied between 2340°F and 2133°F for two cycles. The cycle consisted
of raising the temperature continuously over 11 minutes and lowering the temperature
continuously over 7 minutes.
[0146] After completion of the 2
nd cycle, the induction power supply was placed into manual control. The power was then
instantaneously increased 5 kW above the steady state power level and immediately
upon hitting the 5 kW increased the power was instantaneously decreased back to the
steady state power level. The power level was then varied up 3.7 kW and down 3.7 kW
over 6 cycles. The cycles consisted of raising power 3.7 kW above the steady state
power level over 25 seconds. Once raised, the power level was held at the additional
3.7 kW setting for 45 seconds. Following the 45 second hold, the power was lowered
back to the steady state power level over a 15 second time frame.
[0147] After completion of the 6
th power cycle, the gas flows were adjusted to 0.60 L/min of 100% argon and trace neon
and held for 7 minutes. Following the seven-minute hold, the argon flow was secured
leaving only the trace neon flow. Once the argon flow was secured, a second lance
was positioned inside the reactor. This lance was placed at a distance 2/3 from the
radial center and 1.5 inches from the bottom of the bath. The centerline lance was
then repositioned to ¼ inch from the bottom. Once the centerline lance was repositioned,
flow was started in the off-centerline lance at a rate of 30 ml/min of 100% argon
and trace neon. A timer was initiated. At a time of 2 minutes, the trace neon flow
in the centerline lance was secured. At a time of 2 minutes 30 seconds, flow was initiated
in the centerline lance at a flow rate of 30 ml/min of 100% carbon monoxide and held
for 3 minutes. After the 3-minute hold, flow rates were adjusted in the off-centerline
lance to 0.15 L/min of 100% argon and trace neon and held for 15 minutes. After the
15-minute hold, flow rates were adjusted in the off-centerline lance to trace neon
only. Furthermore, the flow rate was adjusted in the centerline lance to 0.60 L/min
of 100% carbon monoxide and held for 10 minutes. After the 10-minute hold, the carbon
monoxide in the centerline lance was secured. The reactor temperature was then lowered
to T
solidus plus 18°F over 30 minutes. Upon reaching the T
solidus plus 18°F, flow was adjusted in the centerline lance to 0.30 L/min of 100% carbon
monoxide and held for 20 minutes. After the 20-minute hold, all flow was secured in
the centerline lance and the lance was removed.
[0148] After the centerline lance was removed, adjust flow rates in the off-centerline lance
to 30 ml/min of 88% argon, 12% nitrogen and trace neon and held for 3 minutes. After
the 3-minute hold, flow rates were adjusted to 0.30 L/min of 25% helium, 75% argon
and trace neon and held for 10 minutes. After the 10-minute hold, flow rates were
adjusted to 0.30 L/min of 88% argon, 12% nitrogen and trace neon and held for 10 minutes.
After the 10-minute hold, flow rates were adjusted to 0.15 L/min of 88% argon, 12%
nitrogen and trace neon and held for 5 minutes. After the 5-minute hold, flow rates
were adjusted to 30 cc/min of 88% argon, 12% nitrogen and trace neon and held for
2 minutes. After the 2-minute hold, flow rates were adjusted to 0.15 L/min of 88%
argon, 12% nitrogen and trace neon. Once the flow rate was adjusted, the reactor temperature
was lowered to T
solidus plus 15°F over 45 minutes. Upon reaching the T
solidus plus 15°F, flow was adjusted in the off-centerline lance to 0.30 L/min of 100% argon
and trace neon and held for 5 minutes.
[0149] At the completion of five minute hold, the reactor temperature was lowered to T
solidus plus 11°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 11°F, flow rate in the off-centerline lance was adjusted to 0.30 L/min of 100%
hydrogen and trace neon. At the completion of the flow adjustment, the reactor temperature
was then lowered to T
solidus plus 10°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 10°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 100%
hydrogen and trace neon. At the completion of the flow adjustment, the reactor temperature
was lowered to T
solidus plus 9°F while maintaining a temperature-lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 9°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch (1/4 inches) dimple could be observed on the bath surface.
The bath was held at T
solidus plus 9°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. Immediately after the 1.5 kW power pulse, flow was
adjusted in the off-centerline lance to 0.15 L/min of 50% hydrogen, 50% helium and
trace neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 75°F. Upon reaching T
solidus minus 75°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 60%
helium, 40% hydrogen and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.75 kW and the reactor was allowed to cool to
1000°F. Upon reaching 1000°F, flow rate in the off-centerline lance was adjusted to
30 ml/min of 100% helium and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.50 kW and the reactor was allowed to cool to
350°F. Upon reaching 350°F, the induction furnace power supply was shut down and the
timer reinitiated. At a time of 5 minutes, flow rate in the off-centerline lance was
adjusted to 0.60 L/min of 100% helium and trace neon. At a time of 9 minutes, a neon
radiation source within the sealed enclosure was remotely rotated. Upon completion
of the rotation, flow in the off-centerline lance was adjusted to 0.30 L/min of 88%
argon, 12% nitrogen and trace neon.
[0150] Following the flow adjustment, the timer was reinitiated. At a time of 25 seconds,
a neon radiation source within the sealed enclosure was remotely rotated. At a time
of 1 minute 30 seconds, a neon radiation source within the sealed enclosure was terminated.
At a time of 5 minutes an argon radiation source within the sealed enclosure was terminated.
At a time of 6 minute 30 seconds, flow rate was adjusted to 0.30 L/min of 100% helium
and trace neon. At a time of 7 minute, the second neon radiation source within the
sealed enclosure was terminated.
[0151] The timer was reinitiated. At a time of 15 minutes, the trace neon gas flow in the
off-centerline lance was terminated. At a time of 17 minutes 25 seconds, the xenon
radiation source within the sealed enclosure was remotely rotated. At a time of 30
minutes, the trace helium gas flow in the off-centerline lance was terminated. The
timer was reinitiated. At a time of 15 minutes, the xenon radiation source inside
the sealed enclosure was terminated. Thirty minutes were allowed to pass. The ingot
and crucible were removed from the reactor in the presence of radiation sources (metal
halide light sources) utilizing titanium metal tongs.
[0152] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches of DI water. Upon entrance into the quench chamber, a timer was
initiated. At a time of 2 hours 15 minutes, a long wave ultraviolet radiation source
located above the quench vessel was initiated. At a time of 4 hours 7 minutes, a short
wave ultraviolet radiation source located above the quench vessel was initiated. At
a time of 5 hours 59 minutes 30 seconds, the short wave ultraviolet radiation source
located above the quench vessel was rotated to the vertical position.
[0153] At a time of 6 hours, the ingot was removed from the quench system using the titanium
metal tongs and transferred to a clean radiation surface countertop. Exposure to external
radiation sources included the metal halide light and placement directly under a skylight
(which added filtered sunlight to the irradiation sources). The ingot was pat dried.
Upon completion of the drying, the long wave ultraviolet radiation source located
above the quench vessel was rotated vertically and moved up 1 inch. The timer was
then reinitiated. The ingot was irradiated for 10 minutes at which point an additional
radiation source (krypton lamp) was initiated. At 12 minutes 30 seconds, the long
wave ultraviolet radiation source located above the quench vessel was rotated horizontal
and moved down to its original position. At 13 minutes, a xenon radiation source located
above the quench vessel was initiated. At 18 minutes, two orthogonal fluorescent lamp
racks located next to the countertop were turned on. At 30 minutes, two angled metal
halide lights located next to the countertop were simultaneously turned on. At this
point the timer was again reinitiated. At 13 minutes 15 seconds, a neon radiation
source located next to the countertop was turned on. At 15 minutes 30 seconds, an
argon radiation source located next to the countertop was turned on. At 23 minutes
45 seconds, the argon radiation source located next to the countertop was rotated
to an angle of 35°. At 37 minutes 30 seconds, the short wave ultraviolet radiation
source located above the quench vessel was rotated to 35°. At 47 minutes 30 seconds,
the xenon radiation source located above the quench vessel was rotated to horizontal.
At 52 minutes 45 seconds, the long wave ultraviolet radiation source located above
the quench vessel was rotated to 35°. At 58 minutes 30 seconds, the short wave ultraviolet
radiation source located above the quench vessel was rotated to 55°. At 77 minutes,
the krypton radiation source located next to the countertop was rotated to vertical.
At 89 minutes, the krypton radiation source located next to the countertop was rotated
to 78°. At 97 minutes, the krypton radiation source located next to the countertop
was rotated to 88°.
[0154] The timer was reinitiated. At a time of 6 hours, the krypton lamp, short wave ultraviolet,
long wave ultraviolet, argon (located over quench vessel), xenon, argon (located next
to countertop), neon, two orthogonal fluorescent lamp racks, and the two angled metal
halide lights were sequentially terminated in the given order. The timer was again
reinitiated. At a time of 6 hours, 30 minutes, normal lab lighting (metal halides)
was turned off. The timer was reinitiated. For 48 hours, the ingot was allowed to
stabilize with no manual intervention (i.e., no handling).
EXAMPLE 7:
EXPERIMENTAL PROCEDURE FOR COPPER, GOLD, SILVER, RHENIUM ALLOY Method "HD" RUN 14-04-03
[0155] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply. A gas
addition lance was installed to a position approximately ¼ inches from the bottom
of the reactor. The reactor was charged with 9080 g copper (99.98% purity), 7 g rhenium,
5 g silver and 2 g gold through its charging port. The reactor was fitted with a graphite
cap and a ceramic liner (i.e., the crucible, from Engineering Ceramics). During the
entire procedure, a slight positive pressure of 97% argon, 3% hydrogen (~0.5 psig)
was maintained in the reactor using a continuous backspace purge. Bypass injection
of gas addition was commenced (i.e., gas flow diverted around the reactor was initiated)
at a rate of 0.15 L/min of argon. The incoming gas line for the gas addition lance
passes through a sealed, light-tight enclosure whereby irradiation of the gas with
precise radiation sources (e.g., wavelength, intensity, etc) can be achieved. When
the entire gas line had been completely purged (assuming a plug flow model), a neon
radiation source was activated within the sealed enclosure. A timer was set to zero.
Bypass flow was adjusted to 100% argon at a flow rate of 0.15 L/min with trace neon
present (≤ 0.005% vol. to ≤ 5%). At a time of 3 minutes, an argon radiation source
was activated within the sealed enclosure. After completion of another gas line purge
(assuming a plug flow model), the gas line was switched from bypass to direct injection
through the gas addition lance.
[0156] The induction furnace power was then initiated. The reactor was heated to 450°F,
at a rate no greater than 300°F/hr, as limited by the integrity of the crucible. The
induction furnace operated in the frequency range of 0 Hz to 3000 Hz, with frequency
determined by a temperature-controlled feedback loop implementing an Omega Model CN3000
temperature controller. Upon reaching 450°F, the gas addition lance was repositioned
to within 2 inches of the bottom of the reactor. The timer was again set to zero.
At a time of 2 minutes, the gas composition was changed to 0.15 L/min of 66% nitrogen,
34% hydrogen with trace neon present. After completion of another gas line purge (assuming
a plug flow model), a krypton radiation source is initiated in the sealed enclosure.
The reactor heat up continued at a rate no greater than 300°F/hr, as limited by the
integrity of the crucible, until T
solidus minus 30°F was achieved. The gas flow rate was then increased to 0.3 L/min with a
constant gas composition. At T
solidus a second argon radiation source was activated within the sealed enclosure. T
solidus plus 8°F was approached over a 3 to 5 minute time span. From T
solidus plus 8°F to T
solidus plus 15°F, the gas flow rate was reduced to 0.15 L/min with a constant gas composition.
Immediately upon reaching T
solidus plus 15°F, a second neon radiation source was initiated in the sealed enclosure.
Immediately after the second neon radiation source is initiated, the gas composition
is adjusted to 75% hydrogen, 22% nitrogen, and 3% argon with trace neon. The molten
bath was held at this condition for 5 minutes for stabilization.
[0157] After the 5 minute hold, the gas composition was adjusted to 20% helium, 63% nitrogen,
17% argon, and trace neon. The bath was held under these conditions for an additional
15 minutes. Again, following the hold, the gas composition and flow rate were adjusted
to 100% argon with trace neon at a rate of 0.3 L/min. The reactor was held at this
condition for 3 minutes. The timer was reset to zero. At a time of 65 minutes, graphite
saturation assemblies (3/8 inches OD, 36 inches long high purity (<5 ppm impurities)
graphite rods) were inserted to the bottom of the copper alloy charge through ports
located in the top plate. The copper alloy was heated to 2359°F over a 1 hour period.
The bath was then held at this condition for 2 hours. Every 30 minutes during the
hold period, an attempt was made to lower the graphite saturation assemblies as dissolution
occurred. As the copper became saturated with carbon, the graphite saturation assemblies
were consumed. After the 2 hour hold period was complete, the graphite saturation
assemblies were removed. An additional 2.06 grams of graphite powder was charged into
the reactor through the charging port. The bath was then heated to 2474°F over one
hour. Upon achieving 2474°F, the gas composition and flow rate were adjusted to 100%
nitrogen with trace neon at a rate of 0.3 L/min. Hold reactor conditions for 5 minutes.
The gas flow rate was reduced to 0.15 L/min with constant composition. Immediately
following this reduction in gas flow, the krypton radiation source in the sealed enclosure
was turned off. The timer was reset to zero. At a time of 3 minutes, the gas flow
rate was reduced to 37.5 ml/min with constant composition. One of the argon radiation
sources inside the sealed enclosure was turned off. At a time of 5 minutes, the nitrogen
component of the gas flow was discontinued, while maintaining the flow of trace neon.
At a time of 10 minutes, one of the neon radiation sources within the sealed enclosure
was rotated. The reactor temperature is lowered to 2451°F over 7 minutes.
[0158] The temperature was then varied between 2413°F and 2451°F for 16 cycles. Each cycle
consisted of raising the temperature continuously over 7 minutes and lowering the
temperature continuously over 7 minutes. After completion of the 14.5 cycles, argon
was reintroduced at a flow rate of 0.15 L/min with trace neon. Five minutes into the
15
th cycle, a xenon radiation source was activated within the sealed enclosure. At 6 minutes
into the 15
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, a short wave ultraviolet radiation source was initiated in the
sealed enclosure. At sweep count 16, the xenon radiation source was remotely rotated
within the sealed enclosure. The temperature of the copper was varied over another
5 cycles between 2413°F and 2451°F. After the fifth cycle, the reactor temperature
was lowered to 2400°F over a 10 minute period. Upon achieving the target temperature
of 2400, the graphite saturation assemblies were reinstalled in the copper and remained
there for 1 hour. The graphite saturation assemblies were then removed.
[0159] Two voltage probes (source and ground probe) were then installed in the headspace
of the reactor and allowed to equilibrate for 5 minutes. Upon completion of the five
minute hold the voltage probes were lowered into the bath. The source probe was positioned
2 inches below the axial center and 1 inch from the radial center. The ground probe
was positioned 0.75 inches above the axial position of the source probe and 1 inch
from the radial center (180° from the source probe). Once the probes were installed,
a five minute hold at this condition was done to allow the bath to electronically
equilibrate with the probes. Voltage was then applied to the probes and varied between
multiple voltage set points. This voltage application was in a continuous up/down
sweep between two predetermined voltages. The first voltage cycle was varied between
17 and 18 volts for 24 cycles. Each cycle consisted of raising the voltage continuously
over 45 seconds and lowering the voltage continuously over 45 seconds. The second
voltage cycle was varied between 13.25 and 14.75 volts for 20 cycles. Each cycle consisted
of raising the voltage continuously over 45 seconds and lowering the voltage continuously
over 45 seconds. The third voltage cycle was varied between 8.75 and 10.25 volts for
17 cycles. Each cycle consisted of raising the voltage continuously over 45 seconds
and lowering the voltage continuously over 45 seconds. The fourth voltage cycle was
varied between 4.00 and 7.00 volts for 14 cycles. Each cycle consisted of raising
the voltage continuously over 45 seconds and lowering the voltage continuously over
45 seconds. The fifth voltage cycle was varied between 1.50 and 5.00 volts for 10
cycles. Each cycle consisted of raising the voltage continuously over 45 seconds and
lowering the voltage continuously over 45 seconds. The sixth voltage cycle was varied
between 0.50 and 2.00 volts for 3 cycles. Each cycle consisted of raising the voltage
continuously over 45 seconds and lowering the voltage continuously over 45 seconds.
When the final cycle was completed the voltage was set onto a constant 1 volt setting.
This voltage setting remained constant until a later step during which the leads are
removed.
[0160] The reactor temperature was then lowered to 2397°F over 5 minutes. The reactor was
held at this temperature for 5 minutes with continued gas addition. The temperature
was then varied between 2391°F and 2397°F over 20 cycles. Each cycle consisted of
lowering the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. After the 20
th cycle, third body gas addition was changed by turning off the argon component of
the gas leaving only trace neon gas flow. The bath was then cooled to 2388°F over
5 minutes. Upon reaching 2388°F, one of the neon radiation sources was remotely rotated
within the sealed enclosure.
[0161] The temperature was then varied between 2380°F and 2388°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. At sweep count 0.5, a krypton radiation source was initiated in the sealed
enclosure. At sweep count 1.0, an argon radiation source was initiated in the sealed
enclosure. At sweep count 4.5, the short wave ultraviolet radiation source was terminated
in the sealed enclosure. The reactor temperature was then lowered to 2377°F over 5
minutes. The temperature was varied between 2346°F and 2377°F for 15.5 cycles. Each
cycle consisted of lowering the temperature continuously over 15 minutes and raising
the temperature continuously over 15 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. After the 15.5
th cycle, third body gas addition was changed by turning off all gas components except
the trace neon gas flow.
[0162] After the 15.5
th cycle, a timer was started. At a time of 3 minutes, the xenon radiation source was
remotely rotated within the sealed enclosure. The timer was then reset to zero. At
60 minutes, flow rates were adjusted to 0.3 L/min of 100% argon and trace neon. At
65 minutes, flow rates were adjusted to 30 ml/min of 60% argon, 40% helium, and trace
neon. Immediately after the flow was adjusted, one of the neon radiation sources was
remotely rotated within the sealed enclosure. At 68 minutes, flow rates were adjusted
to 0.15 L/min of 100% helium, trace neon, and trace krypton. At 68 minutes 20 seconds,
the 1 volt power was brought to zero output and the voltage power leads removed from
the voltage probes. At 68 minutes 30 seconds, the long wave ultraviolet radiation
source was turned off in the sealed enclosure. At 71 minutes 15 seconds, the voltage
probes were repositioned to three inches above the bath surface. At 75 minutes, the
source and ground probes are removed completely from the reactor.
[0163] After the voltage probes have been removed from the reactor, flow rates were adjusted
to 0.15 L/min of 77% argon, 18% nitrogen, 5% helium and trace neon. The reactor was
then held at temperature and flow rate for 15 minutes. After the 15 minute hold, one
of the argon radiation sources was turned off in the sealed enclosure. The flow rates
were immediately readjusted to 0.15 L/min of 77% argon, 12% nitrogen, 11% helium and
trace neon. The reactor was then held at temperature and flow rate for 25 minutes.
After the 25 minute hold, the krypton radiation source was turned off in the sealed
enclosure. The flow rates were immediately readjusted to 0.30 L/min of 10% argon,
90% helium and trace neon. The reactor was then held at temperature and flow rate
for 3 minutes. After the 3 minute hold, flow rates were adjusted to the flow rate
0.15 L/min of 10% argon, 90% helium and trace neon and held for 2 minutes. After the
2 minute hold, flow rates were adjusted to 0.30 L/min of 7% hydrogen, 93% nitrogen
and trace neon and held for 10 minutes. After the 10 minute hold, flow rates were
adjusted to 0.15 L/min of 7% hydrogen, 93% nitrogen and trace neon and held for 3
minutes. After the 3 minute hold, flow rates were adjusted to 30 ml/min of 7% hydrogen,
93% nitrogen and trace neon and held for 2 minutes. After the 2 minute hold, flow
rates were adjusted to 0.15 L/min of 87% argon, 10% nitrogen, 3% helium and trace
neon and held for 5 minutes. After the 5 minute hold, flow rates were adjusted to
0.6 L/min of 90% argon, 10% nitrogen and trace neon and held for 7 minutes. After
the 7 minute hold, flow rates were adjusted to 30 ml/min of 90% argon, 10% nitrogen
and trace neon and held for 2 minutes. After the 2 minute hold, flow rates were adjusted
to 0.60 L/min of 95% argon, 5% nitrogen and trace neon and held for 15 minutes. After
the 15 minute hold, flow rates were adjusted to 0.30 L/min of 95% argon, 5% nitrogen
and trace neon and held for 5 minutes.
[0164] The reactor temperature was then lowered to 2359°F over 21 minutes. The temperature
was then varied between 2346°F and 2359°F for three cycles. The cycles consisted of
raising the temperature continuously over 27 minutes and lowering the temperature
continuously over 27 minutes. After the third cycle, the bath was held at 2359°F for
5 minutes. The reactor temperature was then lowered to 2346°F over 2 minutes 30 seconds.
The temperature was then varied between 2359°F and 2346°F for two cycles. The cycles
consisted of raising the temperature continuously over 11 minutes and lowering the
temperature continuously over 7 minutes.
[0165] After completion of the 2
nd cycle, the induction power supply was placed into manual control. The power was then
instantaneously increased 5 kW above the steady state power level and immediately
upon hitting the 5 kW, the power was instantaneously decreased back to the steady
state power level. The power level was then varied up 3.7 kW and down 3.7 kW over
6 cycles. The cycles consisted of raising power 3.7 kW above the steady state power
level over 25 seconds. Once raised, the power level was held at the additional 3.7
kW setting for 45 seconds. Following the 45 second hold, the power was lowered back
to the steady state power level over a 15 second time frame.
[0166] After the 6
th power cycle, the gas flows were adjusted to 0.60 L/min of 100% argon and trace neon
and held for 7 minutes. Following the seven minute hold, the argon flow was secured
leaving only the trace neon flow. Once the argon flow was secured, a second lance
was positioned inside the reactor. This lance was placed at a distance 2/3 from the
radial center and 1.5 inches from the bottom of the bath. The centerline lance was
then repositioned to ¼ inch off the bottom. Once the centerline lance was repositioned,
flow was started in the off-centerline lance at a rate of 30 ml/min of 100% argon
and trace neon. A timer was then initiated. At a time of 2 minutes, the trace neon
flow in the centerline lance was discontinued. At a time of 2 minutes 30 seconds,
flow was initiated in the centerline lance at a flow rate of 30 ml/min of 100% carbon
monoxide and held for 3 minutes. After the 3 minute hold, flow rates were adjusted
in the off-centerline lance to 0.15 L/min of 100% argon and trace neon and held for
15 minutes. After the 15 minute hold, flow rates were adjusted in the off-centerline
lance to trace neon only. Furthermore, the flow rate was adjusted in the centerline
lance to 0.60 L/min of 100% carbon monoxide and held for 10 minutes. After the 10
minute hold, the carbon monoxide in the centerline lance was turned off. The reactor
temperature was then lowered to T
solidus plus 18°F over 30 minutes. Upon reaching the T
solidus plus 18°F, flow was adjusted in the centerline lance to 0.30 L/min of 100% carbon
monoxide and held for 20 minutes. After the 20 minute hold, all flow was secured in
the centerline lance and the lance was removed.
[0167] After the centerline lance was removed, flow rates in the off-centerline lance were
adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon and held for 3 minutes.
After the 3 minute hold, flow rates were adjusted to 0.30 L/min of 25% helium, 75%
argon and trace neon and held for 10 minutes. After the 10 minute hold, flow rates
were adjusted to 0.30 L/min of 88% argon, 12% nitrogen and trace neon and held for
10 minutes. After the 10 minute hold, flow rates were adjusted to 0.15 L/min of 88%
argon, 12% nitrogen and trace neon and held for 5 minutes. After the 5 minute hold,
flow rates were adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon and
held for 2 minutes. After the 2 minute hold, flow rates were adjusted to 0.15 L/min
of 88% argon, 12% nitrogen and trace neon. Once the flow rate was adjusted, the reactor
temperature was lowered to T
solidus plus 15°F over 45 minutes. Upon reaching the T
solidus plus 15°F, flow was adjusted in the off-centerline lance to 0.30 L/min of 100% argon
and trace neon and held for 5 minutes.
[0168] At the completion of five minute hold, the reactor temperature was lowered to T
solidus plus 11°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 11°F, flow rate in the off-centerline lance was adjusted to 0.30 L/min of 100%
hydrogen and trace neon. At the completion of the flow adjustment, the reactor temperature
was lowered to T
solidus plus 10°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 10°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 100%
hydrogen and trace neon. At the completion of the flow adjustment, the reactor temperature
was lowered to T
solidus plus 9°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 9°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch (1/4 inches) dimple could be observed on the bath surface.
The bath was held at T
solidus plus 9°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F, a manual power pulse of 1.5 kW was introduced with a single continuous
up/down sweep from normal holding power. Immediately after the 1.5 kW power pulse,
flow was adjusted in the off-centerline lance to 0.15 L/min of 50% hydrogen, 50% helium,
and trace neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 75°F. Upon reaching T
solidus minus 75°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 60%
helium, 40% hydrogen and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.75 kW and the reactor was allowed to cool to
1000°F. Upon reaching 1000°F, flow rate in the off-centerline lance was adjusted to
30 ml/min of 100% helium and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.50 kW and the reactor was allowed to cool to
350°F. Upon reaching 350°F, the induction furnace power supply was shut down and a
timer initiated as time zero (e.g., Timer = T
0). At a time of 5 minutes, flow rate in the off-centerline lance was adjusted to 0.60
L/min of 100% helium and trace neon. At a time of 9 minutes, a neon radiation source
was remotely rotated within the sealed enclosure. Upon completion of the 90° rotation,
flow in the off-centerline lance was adjusted to 0.30 L/min of 88% argon, 12% nitrogen
and trace neon.
[0169] Following the flow adjustment, the timer was reinitiated to time zero. At a time
of 25 seconds, a neon radiation source within the sealed enclosure was remotely rotated.
At a time of 1 minute 30 seconds, a neon radiation source within the sealed enclosure
was turned off. At a time of 5 minutes, an argon radiation source within the sealed
enclosure was turned off. At a time of 6 minute 30 seconds, flow rate was adjusted
to 0.30 L/min of 100% helium and trace neon. At a time of 7 minute, the second neon
radiation source within the sealed enclosure was turned off.
[0170] The timer was reinitiated to time zero (e.g., Timer = T
0). At a time of 15 minutes, the trace neon gas flow in the off-centerline lance was
stopped. At a time of 17 minutes 25 seconds, the xenon radiation source was remotely
rotated 90° within the sealed enclosure. At a time of 30 minutes, the trace helium
gas flow in the off-centerline lance was turned off. The timer was reinitiated to
time zero (e.g., Timer = T
0). At a time of 15 minutes, the xenon radiation source inside the sealed enclosure
was turned off. Thirty minutes were allowed to pass. The ingot and crucible were removed
from the reactor using titanium metal tongs in the presence of light from metal halide
lamps.
[0171] Upon removal from the reactor assembly, the crucible was stripped from the metal
ingot via a gentle wedging action. Immediately following removal, the ingot was transferred
into a quench chamber containing deionized water, ensuring that the top of the ingot
surface was covered by at least 6 inches of deionized (DI) water. Upon immersion into
the quench chamber, a timer was established. At a time of 2 hours 15 minutes, a long
wave ultraviolet radiation source located above the quench vessel was initiated. At
a time of 4 hours 7 minutes, a short wave ultraviolet radiation source located above
the quench vessel was initiated. At a time of 5 hours 59 minutes 30 seconds, the short
wave ultraviolet radiation source located above the quench vessel was rotated to a
vertical position.
[0172] At a time of 6 hours, the ingot was removed from the quench system using the titanium
metal tongs and transferred to a clean radiation surface countertop. Exposure to external
radiation sources included the metal halide light and placement directly under a skylight
(which added filtered sunlight to the irradiation sources). The ingot was pat dried.
Upon completion of the drying, the long wave ultraviolet radiation source located
above the quench vessel was rotated to a vertical position and moved up 1 inch. The
timer was then reset to zero. The ingot was irradiated for 10 minutes at which point
an additional radiation source (krypton lamp) was initiated. At 12 minutes 30 seconds,
the long wave ultraviolet radiation source located above the quench vessel was rotated
and moved down to its original position. At 13 minutes, a xenon radiation source located
above the quench vessel was initiated. At 18 minutes, two orthogonal fluorescent lamp
racks located next to the countertop were turned on. At 30 minutes, two angled metal
halide lights located next to the countertop were simultaneously turned on. At this
point the timer was again reset. At 13 minutes 15 seconds, a neon radiation source
located next to the countertop was turned on. At 15 minutes 30 seconds, an argon radiation
source located next to the countertop was turned on. At 23 minutes 45 seconds, the
argon radiation source located next to the countertop was rotated to an angle of 35°.
At 37 minutes 30 seconds, the short wave ultraviolet radiation source located above
the quench vessel was rotated to 35°. At 47 minutes 30 seconds, the xenon radiation
source located above the quench vessel was rotated to horizontal. At 52 minutes 45
seconds, the long wave ultraviolet radiation source located above the quench vessel
was rotated to 35°. At 58 minutes 30 seconds, the short wave ultraviolet radiation
source located above the quench vessel was rotated to 55°. At 77 minutes, the krypton
radiation source located next to the countertop was rotated to vertical. At 89 minutes,
the krypton radiation source located next to the countertop was rotated to 78°. At
93 minutes, the ingot was lifted using composite black rubber gloves and a tailored
material that acts an energy filter was placed under the ingot. The tailored material
used as an energy filter has an XRF as depicted in Appendix 1. The ingot was then
lowered onto the tailored energy filter. During the installation no direct skin contact
with the ingot was allowed. At 97 minutes, the krypton radiation source located next
to the countertop was rotated to 88°.
[0173] At this point the timer was again reset. At a time of 6 hours, the krypton lamp,
short wave ultraviolet, long wave ultraviolet, argon (located over quench vessel),
xenon, argon (located next to countertop), neon, two orthogonal fluorescent lamp racks,
and the two angled metal halide lights were sequentially terminated in the given order.
The timer was again reset. At a time of 6 hours, 30 minutes, normal lab lighting (metal
halides) was turned off. The timer was reset. For 48 hours, the ingot was allowed
to stabilize with no manual intervention (i.e., no handling).
EXAMPLE 8:
EXPERIMENTAL PROCEDURE FOR COPPER Method "HD" RUN 14-04-05
[0174] A cylindrical alumina-based crucible (99.68% Al
2O
3, 0.07% SiO
2, 0.08% Fe
2O
3, 0.04% CaO, 0.12% Na
2O
3; 4.5 inches O.D. X 3.75 inches I.D. X 14.5 inches depth) of a 100 pound induction
furnace reactor (Inductotherm) fitted with a 73-30R Powertrak power supply. A gas
addition lance was installed to a position approximately ¼ inches from the bottom
of the reactor. The reactor was charged with 9080 g copper (99.98% purity) through
its charging port. The reactor was fitted with a graphite cap and a ceramic liner
(i.e., the crucible, from Engineering Ceramics). During the entire procedure, a slight
positive pressure of 97% argon, 3% hydrogen (~0.5 psig) was maintained in the reactor
using a continuous backspace purge. Bypass injection of gas addition was commenced
(i.e., gas flow diverted around the reactor was initiated) at a rate of 0.15 L/min
of argon. The incoming gas line for the gas addition lance passed through a sealed,
light-tight enclosure whereby irradiation of the gas with precise radiation sources
(e.g., wavelength, intensity, etc) was achieved. When the entire gas line was completely
purged (assuming a plug flow model), a neon radiation source was activated within
the sealed enclosure. A timer was set to zero. Bypass flow was adjusted to 100% argon
at a flow rate of 0.1 L/min with trace neon present. (trace can be defined as ≤ 0.005%
vol. to ≤ 5%). At a time of 3 minutes, an argon radiation source was activated within
the sealed enclosure. After completion of another gas line purge (assuming a plug
flow model), the gas line was switched from bypass to direct injection through the
gas addition lance.
[0175] The induction furnace power was then initiated. The reactor was heated to 450°F,
at a rate no greater than 300°F/hr, as limited by the integrity of the crucible. The
induction furnace operated in the frequency range of 0 Hz to 3000 Hz, with frequency
determined by a temperature-controlled feedback loop implementing an Omega Model CN3000
temperature controller. Upon reaching 450°F, the gas addition lance was repositioned
to 2 inches from the bottom of the reactor. The timer was again set to zero. At a
time of 2 minutes, the gas composition was changed to 0.15 L/min of 66% nitrogen,
34% hydrogen with trace neon present. After completion of another gas line purge (assuming
a plug flow model), a krypton radiation source was initiated in the sealed enclosure.
The reactor heat up was continued at a rate no greater than 300°F/hr, as limited by
the integrity of the crucible, until T
solidus minus 30°F was achieved. The gas flow rate was then increased to 0.3 L/min with a
constant gas composition. At T
solidus a second argon radiation source was activated within the sealed enclosure. T
solidus plus 8°F was approached over a 3 to 5 minute time span. From T
solidus plus 8°F to T
solidus plus 15°F, the gas flow rate was reduced to 0.15 L/min with a constant gas composition.
Immediately upon reaching T
solidus plus 15°F, a second neon radiation source was initiated in the sealed enclosure.
Immediately after the second neon radiation source was initiated, the gas composition
was adjusted to 75% hydrogen, 22% nitrogen, 3% argon and trace neon. The molten bath
was held at this condition for 5 minute for stabilization.
[0176] After the 5 minute hold, the gas composition was adjusted to 20% helium, 63% nitrogen,
17% argon, and trace neon. The bath was held under these conditions for an additional
15 minutes. Again, following the hold, the gas composition and flow rate were adjusted
to 100% argon with trace neon at a rate of 0.3 L/min. The reactor was held at this
condition for 3 minutes. The timer was reset to zero. At a time of 65 minutes, graphite
saturation assemblies (3/8 inches OD, 36 inches long high purity (<5 ppm impurities)
graphite rods) were inserted to the bottom of the copper charge through ports located
in the top plate. The copper was heated to 2359°F over a one hour period. The bath
was then held at this condition for 2 hours. Every 30 minutes during the hold period,
an attempt was made to lower the graphite saturation assemblies as dissolution occurred.
As the copper became saturated with carbon, the graphite saturation assemblies were
consumed. After the 2 hour hold period was complete, the graphite saturation assemblies
were removed. An additional 2.06 grams of graphite powder was charged into the reactor
through the charging port. The bath was then heated to 2474°F over one hour. Upon
achieving 2474°F, the gas composition and flow rate were adjusted to 100% nitrogen
with trace neon at a rate of 0.3 L/min. The reactor conditions were held for 5 minutes.
The gas flow rate was reduced to 0.15 L/min with constant composition. Immediately
following this reduction in gas flow, the krypton radiation source in the sealed enclosure
was turned off. The timer was reset to zero. At a time of 3 minutes, the gas flow
rate was reduced to 37.5 ml/min with constant composition. One of the argon radiation
sources inside the sealed enclosure was turned off. At a time of 5 minutes, the nitrogen
component of the gas flow was discontinued, while maintaining the flow of the trace
neon. At a time of 10 minutes, one of the neon radiation sources was remotely rotated
(90°) within the sealed enclosure. The reactor temperature was lowered to 2451°F over
7 minutes.
[0177] The temperature was then varied between 2413°F and 2451°F for 16 cycles. Each cycle
consisted of raising the temperature continuously over 7 minutes and lowering the
temperature continuously over 7 minutes. After completion of the 14.5 cycles, argon
was reintroduced at a flow rate of 0.15 L/min with trace neon. Five minutes into the
15
th cycle, a xenon radiation source was activated within the sealed enclosure. At 6 minutes
into the 15
th cycle, a long wave ultraviolet radiation source was activated in the sealed enclosure.
At sweep count 15.5, a short wave ultraviolet radiation source was initiated in the
sealed enclosure. At sweep count 16, remotely rotate the xenon radiation source within
the sealed enclosure. The temperature of the copper was varied over another 5 cycles
between 2413°F and 2451°F. After the fifth cycle, the reactor temperature was lowered
to 2400°F over a 10 minute period. Upon achieving the target temperature of 2400,
the graphite saturation assemblies were reinstalled in the copper and remained there
for 1 hour. The graphite saturation assemblies were then removed.
[0178] Two voltage probes (source and ground probe) were then installed in the headspace
of the reactor and allowed to equilibrate for 5 minutes. Upon completion of the five
minute hold the voltage probes were lowered into the bath. The source probe should
be positioned 2 inches below the axial center and 1 inch from the radial center. The
ground probe was positioned 0.75 inches above the axial position of the source probe
and 1 inch from the radial center (180° from the source probe). Once the probes were
installed a five minute hold at this condition was done to allow the bath to electronically
equilibrate with the probes. Voltage was then applied to the probes and varied between
multiple voltage set points. This voltage application was in a continuous up/down
sweep between two predetermined voltages. The first voltage cycle was varied between
17 and 18 volts for 24 cycles. Each cycle consisted of raising the voltage continuously
over 45 seconds and lowering the voltage continuously over 45 seconds. The second
voltage cycle was varied between 13.25 and 14.75 volts for 20 cycles. Each cycle consisted
of raising the voltage continuously over 45 seconds and lowering the voltage continuously
over 45 seconds. The third voltage cycle was varied between 8.75 and 10.25 volts for
17 cycles. Each cycle consisted of raising the voltage continuously over 45 seconds
and lowering the voltage continuously over 45 seconds. The fourth voltage cycle was
varied between 4.00 and 7.00 volts for 14 cycles. Each cycle consisted of raising
the voltage continuously over 45 seconds and lowering the voltage continuously over
45 seconds. The fifth voltage cycle was varied between 1.50 and 5.00 volts for 10
cycles. Each cycle consisted of raising the voltage continuously over 45 seconds and
lowering the voltage continuously over 45 seconds. The sixth voltage cycle was varied
between 0.50 and 2.00 volts for 3 cycles. Each cycle consisted of raising the voltage
continuously over 45 seconds and lowering the voltage continuously over 45 seconds.
When the final cycle was completed the voltage was set onto a constant 1 volt setting.
This voltage setting remains constant until a later step during which the leads are
removed.
[0179] The reactor temperature was lowered to 2397°F over 5 minutes. The reactor was held
at this temperature for 5 minutes with continued gas addition. The temperature was
then varied between 2391°F and 2397°F over 20 cycles. Each cycle consisted of lowering
the temperature continuously over 9 minutes and raising the temperature continuously
over 9 minutes. After the 20
th cycle, third body gas addition was changed by turning off the argon component of
the gas leaving only trace neon gas flow. The bath was then cooled to 2388°F over
5 minutes. Upon reaching 2388°F, remotely rotate one of the neon radiation sources
within the sealed enclosure.
[0180] The temperature was then varied between 2380°F and 2388°F over 4.5 cycles. Each cycle
consisted of lowering the temperature continuously over 5 minutes and raising the
temperature continuously over 3 minutes. In addition, while raising the temperature,
a 0.15 L/min flow of 60% argon, 40% helium, and trace neon was added, and while lowering
the temperature, a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was
added. At sweep count 0.5, a krypton radiation source was initiated in the sealed
enclosure. At sweep count 1.0, an argon radiation source was initiated in the sealed
enclosure. At sweep count 4.5, the short wave ultraviolet radiation source was terminated
in the sealed enclosure. The reactor temperature was lowered to 2377°F over 5 minute.
The temperature was varied between 2346°F and 2377°F for 15.5 cycles. Each cycle consisted
of lowering the temperature continuously over 15 minutes and raising the temperature
continuously over 15 minutes. In addition, while raising the temperature, a 0.15 L/min
flow of 60% argon, 40% helium, and trace neon was added, and while lowering the temperature,
a 0.3 L/min flow of 100% helium, trace neon, and trace krypton was added. After the
15.5
th cycle, third body gas addition was changed by turning off all gas components except
the trace neon gas flow.
[0181] After the 15.5
th cycle, a timer was established. At a time of 3 minutes, the xenon radiation source
was rotated 90° within the sealed enclosure. The timer was then reset to zero. At
60 minutes, flow rates were adjusted to 0.3 L/min of 100% argon and trace neon. At
65 minutes, flow rates were adjusted to 30 ml/min of 60% argon, 40% helium, and trace
neon. Immediately after the flow was adjusted, one of the neon radiation sources was
remotely rotated 90° within the sealed enclosure. At 68 minutes, flow rates were adjusted
to 0.15 L/min of 100% helium, trace neon and trace krypton. At 68 minutes 20 seconds,
the 1 volt power was brought to zero output and the voltage power leads removed from
the voltage probes. At 68 minutes 30 seconds, the long wave ultraviolet radiation
source was turned off in the sealed enclosure. At 71 minutes 15 seconds, the voltage
probes were repositioned to three inches above the bath surface. At 75 minutes, the
source and ground probes were removed completely from the reactor.
[0182] After the voltage probes had been removed from the reactor, flow rates were adjusted
to 0.15 L/min of 77% argon, 18% nitrogen, 5% helium and trace neon. The reactor was
then held at temperature and flow rate for 15 minutes. After the 15 minute hold, an
argon radiation source was turned off in the sealed enclosure. The flow rates were
immediately readjusted to 0.15 L/min of 77% argon, 12% nitrogen, 11% helium and trace
neon. The reactor was then held at temperature and flow rate for 25 minutes. After
the 25 minute hold, the krypton radiation source was turned off in the sealed enclosure.
The flow rates were immediately readjusted to 0.30 L/min of 10% argon, 90% helium
and trace neon. The reactor was then held at temperature and flow rate for 3 minutes.
After this 3 minute hold, flow rates were adjusted to 0.15 L/min of 10% argon, 90%
helium and trace neon and held for 2 minutes. After this 2 minute hold, flow rates
were adjusted to 0.30 L/min of 7% hydrogen, 93% nitrogen and trace neon and held for
10 minutes. After this 10 minute hold, flow rates were adjusted to 0.15 L/min of 7%
hydrogen, 93% nitrogen and trace neon and held for 3 minutes. After this 3 minute
hold, flow rates were adjusted to 30 ml/min of 7% hydrogen, 93% nitrogen and trace
neon and held for 2 minutes. After this 2 minute hold, flow rates were adjusted to
0.15 L/min of 87% argon, 10% nitrogen, 3% helium and trace neon and held for 5 minutes.
After this 5 minute hold, flow rates were adjusted to 0.6 L/min of 90% argon, 10%
nitrogen and trace neon and held for 7 minutes. After this 7 minute hold, flow rates
were adjusted to 30 ml/min of 90% argon, 10% nitrogen and trace neon and held for
2 minutes. After this 2 minute hold, flow rates were adjusted to 0.60 L/min of 95%
argon, 5% nitrogen and trace neon and held for 15 minutes. After this 15 minute hold,
flow rates were adjusted to 0.30 L/min of 95% argon, 5% nitrogen and trace neon and
held for 5 minutes.
[0183] The reactor temperature was then lowered to 2359°F over 21 minutes. The temperature
was then varied between 2346°F and 2359°F for three cycles. The cycles consisted of
raising the temperature continuously over 27 minutes and lowering the temperature
continuously over 27 minutes. After the third cycle, the bath was held at 2359°F for
5 minutes. The reactor temperature was then lowered to 2346°F over 2 minutes 30 seconds.
The temperature was then varied between 2359°F and 2346°F for two cycles. The cycles
consisted of raising the temperature continuously over 11 minutes and lowering the
temperature continuously over 7 minutes.
[0184] After the completion of the 2
nd cycle, the induction power supply was placed into manual control. The power was then
instantaneously increased 5 kW above the steady state power level and immediately
upon hitting the 5kW increase the power was instantaneously decreased back to the
steady state power level. The power level was then varied up 3.7 kW and down 3.7 kW
over 6 cycles. The cycles consisted of raising power 3.7 kW above the steady state
power level over 25 seconds. Once raised, the power level was held at the additional
3.7 kW setting for 45 seconds. Following the 45 second hold, the power was lowered
back to the steady state power level over a 15 second time frame.
[0185] After the 6
th power cycle, the gas flows were adjusted to 0.60 L/min of 100% argon and trace neon
and held for 7 minutes. Following the seven minute hold, the argon flow was turned
off leaving only the trace neon flow. Once the argon flow was turned off, a second
lance was positioned inside the reactor. This lance should be placed at a position
2/3 of the distance from the radial center and 1.5 inches from the bottom of the bath.
The centerline lance was then repositioned to ¼ inch from the bottom. Once the centerline
lance was repositioned, flow was started in the off-centerline lance at a rate of
30 ml/min of 100% argon and trace neon. A timer was then initiated at zero (e.g.,
Timer = T
0). At a time of 2 minutes, the trace neon flow in the centerline lance was stopped.
At a time of 2 minutes 30 seconds, flow was initiated in the centerline lance at a
flow rate of 30 ml/min of 100% carbon monoxide and held for 3 minutes. After the 3
minute hold, flow rates were adjusted in the off-centerline lance to 0.15 L/min of
100% argon and trace neon and held for 15 minutes. After the 15 minute hold, flow
rates were adjusted in the off-centerline lance to trace neon only. Furthermore, the
flow rate was adjusted in the centerline lance to 0.60 L/min of 100% carbon monoxide
and held for 10 minutes. After the 10 minute hold, the carbon monoxide in the centerline
lance was turned off. The reactor temperature was then lowered to T
solidus plus 18°F over 30 minutes. Upon reaching the T
solidus plus 18°F, flow was adjusted in the centerline lance to 0.30 L/min of 100% carbon
monoxide and held for 20 minutes. After the 20 minute hold, all flow was discontinued
in the centerline lance and the lance was removed.
[0186] After the centerline lance was removed, flow rates are adjusted in the off-centerline
lance to 30 ml/min of 88% argon, 12% nitrogen and trace neon and held for 3 minutes.
After the 3 minute hold, flow rates were adjusted to 0.30 L/min of 25% helium, 75%
argon and trace neon and held for 10 minutes. After the 10 minute hold, flow rates
were adjusted to 0.30 L/min of 88% argon, 12% nitrogen and trace neon and held for
10 minutes. After the 10 minute hold, flow rates were adjusted to 0.15 L/min of 88%
argon, 12% nitrogen and trace neon and held for 5 minutes. After the 5 minute hold,
flow rates were adjusted to 30 ml/min of 88% argon, 12% nitrogen and trace neon and
held for 2 minutes. After the 2 minute hold, flow rates were adjusted to 0.15 L/min
of 88% argon, 12% nitrogen and trace neon. Once the flow rate was adjusted, the reactor
temperature was then lowered to T
solidus plus 15°F over 45 minutes. Upon reaching the T
solidus plus 15°F, flow was adjusted in the off-centerline lance to 0.30 L/min of 100% argon
and trace neon and held for 5 minutes.
[0187] At the completion of the 5 minute hold, the reactor temperature was then lowered
to T
solidus plus 11°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 11°F, the flow rate in the off-centerline lance was adjusted to 0.30 L/min of
100% hydrogen and trace neon. At the completion of the flow adjustment, the reactor
temperature was then lowered to T
solidus plus 10°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 10°F, the flow rate in the off-centerline lance was adjusted to 30 ml/min of
100% hydrogen and trace neon. At the completion of the flow adjustment, the reactor
temperature was lowered to T
solidus plus 9°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 9°F, the gas addition lance was relocated into the headspace of the reactor,
such that a quarter inch (1/4 inches) dimple could be observed on the bath surface.
The bath was held at T
solidus plus 9°F for an additional 5 minutes for conditioning and equilibration. The reactor
was then cooled to T
solidus plus 8°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 8°F a manual power pulse of 2 kW was introduced with a single continuous up/down
sweep from normal holding power. The reactor was then cooled to T
solidus plus 2°F while maintaining a temperature lowering rate of no more than 3°F/hr. Upon
reaching T
solidus plus 2°F a manual power pulse of 1.5 kW was introduced with a single continuous up/down
sweep from normal holding power. Immediately after the 1.5 kW power pulse, flow was
adjusted in the off-centerline lance to 0.15 L/min of 50% hydrogen, 50% helium and
trace neon. The reactor was then cooled to T
solidus again maintaining a temperature-lowering rate of no more than 3°F/hr. Upon reaching
T
solidus, the induction furnace power supply was lowered to 1 kW and the reactor was allowed
to cool from T
solidus to T
solidus minus 75°F. Upon reaching T
solidus minus 75°F, flow rate in the off-centerline lance was adjusted to 30 ml/min of 60%
helium, 40% hydrogen and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.75 kW and the reactor was allowed to cool to
1000°F. Upon reaching 1000°F, flow rate in the off-centerline lance was adjusted to
30 ml/min of 100% helium and trace neon. Following the flow adjustment, the induction
furnace power supply was lowered to 0.50 kW and the reactor was allowed to cool to
350°F. Upon reaching 350°F, the induction furnace power supply was shut down and a
timer initiated at time zero. At a time of 5 minutes, flow rate in the off-centerline
lance was adjusted to 0.60 L/min of 100% helium and trace neon. At a time of 9 minutes,
a neon radiation source within the sealed enclosure was remotely rotated 90°. Upon
completion of the rotation, flow in the off-centerline lance was adjusted to 0.30
L/min of 88% argon, 12% nitrogen and trace neon.
[0188] Following the flow adjustment, reinitiate the timer to zero. At a time of 25 seconds,
remotely rotate a neon radiation source within the sealed enclosure (90°). At a time
of 1 minute 30 seconds, a neon radiation source within the sealed enclosure was turned
off. At a time of 5 minutes, a argon radiation source within the sealed enclosure
was turned off. At a time of 6 minute 30 seconds, flow rate was adjusted to 0.30 L/min
of 100% helium and trace neon. At a time of 7 minute, the second neon radiation source
within the sealed enclosure was turned off.
[0189] The timer was reinitiated to time zero. At a time of 15 minutes, the trace neon gas
flow in the off-centerline lance was turned off. At a time of 17 minutes 25 seconds,
the xenon radiation source within the sealed enclosure was remotely rotated 90°. At
a time of 30 minutes, the trace helium gas flow in the off-centerline lance was turned
off. The timer was reinitiated to time zero. At a time of 15 minutes, the xenon radiation
source inside the sealed enclosure was turned off. Thirty minutes were allowed to
pass. The ingot and crucible were removed from the reactor in the presence of radiation
sources (metal halide light sources) utilizing titanium metal tongs.
[0190] Upon removal, the crucible was stripped from the metal ingot via a gentle wedging
action. Immediately following removal, the ingot was transferred into a quench chamber
containing deionized water, ensuring that the top of the ingot surface was covered
by at least 6 inches of DI water. Upon entrance into the quench chamber, a timer was
established at time zero. At a time of 2 hours 15 minutes, a long wave ultraviolet
radiation source located above the quench vessel was initiated. At a time of 4 hours
7 minutes, a short wave ultraviolet radiation source located above the quench vessel
was initiated. At a time of 5 hours 59 minutes 30 seconds, the short wave ultraviolet
radiation source located above the quench vessel was rotated (90°) to a tip up position.
[0191] At a time of 6 hours, the ingot was removed from the quench system using the titanium
metal tongs and transferred to a clean radiation surface countertop. Exposure to external
radiation sources included the metal halide light and placement directly under a skylight
(which added filtered sunlight to the irradiation sources). The ingot was pat dried.
Upon completion of the drying, the long wave ultraviolet radiation source located
above the quench vessel was rotated to a vertical orientation and moved up 1 inch.
The timer was then reset to zero. The ingot was irradiated for 10 minutes at which
point an additional radiation source (krypton lamp) was initiated. At 12 minutes 30
seconds, the long wave ultraviolet radiation source located above the quench vessel
was rotated (90°) and moved down to its original position. At 13 minutes, a xenon
radiation source located above the quench vessel was initiated. At 18 minutes, two
orthogonal fluorescent lamp racks located next to the countertop were turned on. At
30 minutes, two angled metal halide lights located next to the countertop were simultaneously
turned on. At this point the timer was again reset to zero. At 13 minutes 15 seconds,
a neon radiation source located next to the countertop was turned on. At 15 minutes
30 seconds, an argon radiation source located next to the countertop was turned on.
At 23 minutes 45 seconds, the argon radiation source located next to the countertop
was rotated to an angle of 35°. At 37 minutes 30 seconds, rotate the short wave ultraviolet
radiation source located above the quench vessel to 35°. At 47 minutes 30 seconds,
the xenon radiation source located above the quench vessel was rotated to a horizontal
orientation. At 52 minutes 45 seconds, the long wave ultraviolet radiation source
located above the quench vessel was rotated to 35°. At 58 minutes 30 seconds, the
short wave ultraviolet radiation source located above the quench vessel was rotated
to 55°. At 77 minutes, the krypton radiation source located next to the countertop
was rotated to a vertical orientation. At 89 minutes, the krypton radiation source
located next to the countertop was rotated to 78°. At 93 minutes, the ingot was lifted
using composite black rubber gloves and a tailored material that acts as an energy
filter was placed under the ingot. The tailored material used as an energy filter
has an XRF as depicted in Appendix 1. The ingot was then lowered onto the tailored
energy filter. At 97 minutes, the krypton radiation source located next to the countertop
was rotated to 88°.
[0192] At this point the timer was again reset to zero. At a time of 6 hours, the krypton
lamp, short wave ultraviolet, long wave ultraviolet, argon (located over quench vessel),
xenon, argon (located next to countertop), neon, two orthogonal fluorescent lamp racks,
and the two angled metal halide lights were sequentially turned off in the given (aforementioned)
order. The timer was again reset to zero. At a time of 6 hours, 30 minutes, normal
lab lighting (metal halides) was turned off. The timer was reset to zero. For 48 hours,
the ingot was allowed to stabilize with no manual intervention (i.e., no handling).
Analytical Protocols:
X-ray Fluorescence
[0193] An ARL 8410 XRF was used to analyze each of the sample ingots. An ARL 8410 is a sequential
wavelength dispersive spectrometer (WDS). Specific emission lines are used to determine
the presence or absence, and the concentrations of various elements. Each characteristic
x-ray line is measured in sequence by the instrument by controlling the instrument
geometry.
[0194] The ARL 8410 (WDS) spectrometer relies on the fundamentals of x-ray diffraction.
X-ray fluorescence occurs when matter is bombarded by a stream of high-energy incident
x-ray photons. When the incident X-radiation strikes the sample, the incident x-rays
may be absorbed, scattered, or transmitted for the measurement of the fluorescent
yield.
[0195] The ARL 8410 utilizes an end-window rhodium (Rh) x-ray tube. The end-window is composed
of beryllium, and holds the tube at high vacuum. The filaments are heated giving off
electrons by thermoionic emission. This beam of electrons then bombards the target
Rh anode across a 10-70 keV voltage potential. Thus, primary x-rays are produced during
the collision. The emitted x-ray spectrum consists of (1) "Continuum" or "Bremstrahlung"
radiation, (2) Characteristic x-ray lines of the target material (e.g., K and L series),
and (3) Characteristic lines from any contaminants. Thus, the primary spectrum appears
as a series of sharp intense peaks arrayed over a broad hump of continuum radiation.
The ARL is equipped with and uses two types of photon detectors, the Flow Proportional
Counter (FPC) and the Scintillation Counter (SC).
[0196] The manufactured metal samples, unless otherwise specified, are prepared by cutting
a sample with an approximate cross-section of 1.1875" from the cooled ingot. The axial
edge and radial edge are then denoted. For non-brittle samples, a cube-shaped sample
is used. When possible, a smooth surface is prepared for analysis; the axial and radial
faces are sequentially polished. The sample faces are sanded to 400 grit and then
a polishing wheel is employed with 600 grit paper. Finally, a 1 µm polishing compound
completes the smoothing process.
[0197] Prior to analysis, the sample is cleaned with isopropyl alcohol (IPA) and placed
in a sample cassette/holder. The sample holder is then loaded into the XRF.
[0198] The orientation of the detector crystal with respect to the sample and the photon
detector is controlled synchronously such that characteristic x-ray lines can be accurately
measured. A sequential measurement consists of positioning the diffraction crystal
at a given theta (diffraction angle) and the detector at two-theta and counting for
a given period of time. The crystal and detector are then rotated to a different angle
for the next characteristic x-ray line.
[0199] XRF 386 Software by Fisons Instruments is used to control the crystal and detector
placement. Uniquant Version 2 software, developed by Omega Data Systems provides the
data reduction algorithms for each analytical protocol. The sample results include
an elemental composition list along with the associated concentrations for each sample.
Measurement of Magnetism and Material Attraction
[0200] The magnetic and material attraction properties of the manufactured ingots were tested
via four methods:
Magnetic Attraction: An 1/8 inch diameter (0.0625 inch thick) neodymium iron boron magnet (NdFeB) was
scanned consistently and uniformly across the surface of the ingot to detect areas
of attraction. Areas of attraction were then noted at specific sites on the surface
in both a vertical and horizontally inverted (i.e., upside down) orientation.
Attraction to Iron: The attraction of iron chips (99%wt purity; between 10 and 25 mesh), iron powder (94%wt Fe, 3%wt C, 3%wt S), and spherical sponge iron (99.8%wt purity, -50 to +100 mesh) to specific areas on the tailored ingots was observed and recorded. The
retention of the iron media (chips, sponge balls, or powder) on the ingot surface
was observed in a vertical and horizontally inverted (i.e., upside-down) orientation.
Gauss Measurement: An F. W. Bell 4048 Gauss meter was used to perform precise measurements of the magnetic
fields observable across the surfaces of the ingots. A scan of each face was performed
to create grids of the magnetic force. These scans provide an indication of the magnetic
flux density, the property of magnetic fields that determines the force that is exerted
upon a current or moving charge. Hence, a large magnetic field measurement should
be indicative of strong attraction and conversely no magnetic field measurement should
be indicative of no attraction. The magnetic behavior of various points on the ingot
were specifically quantified to note that even though they exhibited clear magnetic
attraction, an insignificant Gauss reading was observed (e.g., comparable to the background
magnetic field measured at the earth's surface).
Non-magnetic Attraction: Many of the manufactured materials were found to exhibit unique attraction to non-magnetic,
non-ferromagnetic materials. For example, sulfur powder was shown to exhibit an attraction
to the surface of the tailored ingots. The sulfur powder (99.9% purity, 20 mesh) was
spread evenly over the surface of the clean, polished, dry manufactured ingot. The
ingot was then rotated to a vertical position (90° to the ground). The retention of
powder was documented via photography and manual mapping in a lab notebook. The sample
was inverted completely (180° rotation from its resting position on the surface).
Again, powder retention was documented. This procedure was repeated on both the top
and bottom surfaces of the manufactured ingot.
Hardness
[0201] Hardness testing was performed via multiple techniques, including Moh's hardness
testing and Rockwell hardness testing (both standard techniques). In Moh's hardness
testing the test angle approaches 0°, while in Rockwell testing the test angle approaches
90°. By testing at multiple angles, changes to different contributing aspects of changing
the composition of matter could be tested.
[0202] The Rockwell method (ASTM 18-84 Standard Test Methods for Rockwell Hardness and Rockwell
Superficial Hardness of Metallic Materials) employs either a ball or a diamond cone
in a precision-testing instrument that is designed to measure depth of penetration
accurately. Two superimposed impressions are made, one with a load of 10 kg and the
second with a load of 100 kg. The depth to which the major load drives the ball or
cone below that depth to which the minor load has previously driven it is taken as
a measure of the hardness. For hardened steels, greater accuracy is obtained by using
a diamond cone (120° with slightly rounded tip) applied under a major load of 150
kg. The Rockwell hardness test B uses the 1/16" diameter steel ball with a 100 kg
load. Scale B is appropriate for copper alloys, soft steels, aluminum alloys, malleable
iron, etc.; Scale C is appropriate for steel, hard cast irons, pearlitic malleable
iron, titanium, deep case hardened steel and other materials harder than B 100. The
method using the cone is designated Rockwell C test. Based on the depth of the indentation,
the hardness scale can be read directly from the scale, the higher the number, the
harder the material. The dial-like scale is really a depth gauge, graduated in special
units specific to the test being performed, e.g., Rockwell Hardness C.
[0203] The Rockwell results are a useful measure of relative resistance to indentation;
however, the Rockwell test does not serve well as a predictor of other properties
such as strength or resistance to scratches, abrasion, or wear. Hence, the Rockwell
hardness test cannot be used alone for product specifications.
[0204] The Moh's Scales, in use since 1822, is used to rank the relative hardness of minerals
via the ability of materials to resist scratching by another material. Moh's scale
consists of 10 minerals arranged in order from 1 to 10. Diamond is rated as the hardest
and is indexed as 10. Talc is indexed as 1 and is the softest. Each mineral in the
scale will scratch those below it:
Mineral |
Index |
Diamond |
10 |
Corundum |
9 |
Topaz |
8 |
Quartz |
7 |
Orthoclase (Feldspar) |
6 |
Apatite |
5 |
Fluorite |
4 |
Calcite |
3 |
Gypsum |
2 |
Talc |
1 |
[0205] The steps are not of equal value (i.e., nonlinear) and the difference in hardness
between 9 and 10 is much greater than between 1 and 2 (i.e., step size approaches
an exponential function). The hardness is determined by finding which of the standard
minerals the test material will scratch or not scratch; the hardness will lie between
two points on the scale-the first point being the mineral which is scratched and the
next point being the mineral which is not scratched. In the determination procedure,
it is necessary to be certain that a scratch is actually made and not just a "chalk"
mark that will rub off. Natural copper is between 2 and 3 and tool steel is between
6 and 7.
Appearance/Color
[0206] The color of each sample is noted via visual evaluation. In addition, unique surface
configurations are documented (for example, the expulsion of material from the bath
upon cooling). Digital photography is used to document the physical appearance.
Results:
[0207] The following is a list of manufactured materials prepared by the techniques described
herein and the ingot compositions.
Table 1: Manufactured Ingots Prepared via Specified Technique
Experimental Protocol/Method |
Experimental Run Number |
Metal |
Quantity (grams) |
Purity (wt %) |
"AB" (Example 1) |
14-03-02 |
Copper |
9080 |
99.98 |
"AB" without EM radiation |
14-03-03 |
Copper |
9080 |
99.98 |
"AB" |
14-01-10 |
Aluminum |
3454 |
99.9 |
"AB" |
14-01-11 |
Aluminum |
3454 |
99.9 |
"HA" (Example 2) |
14-02-06 |
Copper |
9080 |
99.98 |
"HA" (Example 3) |
14-04-02 |
Aluminum |
4540 |
99.99 |
"HD" (Example 4) |
14-01-20 |
Cobalt |
8899 |
99.5 |
|
Vanadium |
182 |
99.5 |
|
Rhenium |
7 |
99.997 |
"HD" (Example 5) |
14-01-21 |
Nickel |
9080 |
99.97 |
|
Rhenium |
5 |
99.997 |
"HD" (Example 6) |
14-01-13 |
Iron |
8534 |
99.98 |
|
Vanadium |
182 |
99.5 |
|
Chromium |
182 |
99.999 |
|
Manganese |
182 |
99.99 |
"HD" (Example 7) |
14-04-03 |
Copper |
9080 |
99.98 |
|
Rhenium |
7 |
99.997 |
|
Silver |
5 |
99.99 |
|
Gold |
2 |
99.99 |
"HD" (Example 8) |
14-04-05 |
Copper |
9080 |
99.98 |
"HD" with modulated cool down |
14-01-15 |
Iron |
8534 |
99.98 |
|
Vanadium |
182 |
99.5 |
|
Chromium |
182 |
99.999 |
|
Manganese |
182 |
99.99 |
"HD" with modulated EM radiation |
14-02-03 |
Iron |
9973.4 |
99.98 |
|
Vanadium |
212.2 |
99.5 |
|
Chromium |
212.2 |
99.999 |
|
Manganese |
212.2 |
99.99 |
"HD" with modulated (EM radiation) angle of incidence |
14-04-06 |
Copper |
9080 |
99.98 |
XRF Results:
[0208] Appendix 2 shows tables of XRF data results for the manufactured materials. Note
in each table the apparent detection of materials not present in the initial starting
materials. Such detections are indicative of a shift in the energy of the manufactured
materials, manifesting itself in "false positives" for the detection of elements not
present.
[0209] In addition, despite the fact that the manufactured ingots were prepared in a very
well-mixed reactor, where composition should be homogeneous, significant "apparent"
compositional differences exist in the axial and radial directions. Note XRF data
for each ingot is presented in back-to-back tables in Appendix 2. This anisotropic
behavior is again indicative of changes in the energy patterning of the manufactured
materials.
[0210] Such shifts in energy are demonstrated best in identical experiments that were performed
manufacturing copper (Runs 14-03-02 and 14-03-03). The primary difference in these
two experimental runs was to perform electromagnetic (EM) energy addition to the third-body
gases prior to injection into the reactor. The XRF results for these experiments are
summarized below in Table 2:
Table 2: XRF Results Summary for 14-03-02 and 14-03-03
Element (wt %) |
14-03-02 (EM radiation addition through third-body gases) |
14-03-03 |
|
Axial |
Radial |
Axial |
Radial |
Cu |
97.95 |
99.03 |
99.55 |
99.23 |
Al |
1.79 |
0.79 |
0.23 |
0.29 |
Si |
0.111 |
- |
0.038 |
0.27 |
La |
0.012 |
- |
0.02 |
- |
Pr |
0.005 |
- |
- |
0.006 |
Gd |
- |
- |
0.003 |
0.003 |
Er |
- |
0.008 |
0.013 |
0.017 |
ΣConc. |
99.8 |
99.5 |
99.0 |
99.3 |
[0211] Note the differences in axial and radial concentrations; the detection of elements
not present in any of the initial feed materials or reactor materials; and the differences
in experimental results for identical experimental programs except for the addition
of EM radiation through third-body gases.
Physical Appearance and Color
[0212] Visual inspection of the manufactured materials indicates that the physical characteristics
of the material have been dramatically altered. Major physical changes can include
color, texture, the appearance of void spaces in the ingot internals, the expulsion
of metal during the cooling process, and apparent volumetric changes.
[0213] Comparison of ingots of similar composition, but manufactured via alternate techniques,
can exemplify the physical manifestations of changes to the composition of matter.
The exterior volume of ingot 14-04-01 (Example 1 of
USSN 10/123,028, substituting Al for Cu) is significantly greater (~30%) than 14-04-02 with an internal
void in the ingot that runs approximately 80% down the length of the ingot. Interestingly,
the ingot 14-04-01 was subjected to lower volumetric gas flow rates than ingot 14-04-02;
hence gas expansion is not a plausible explanation for the physical differences. Additionally,
the ingot prepared via the subject method exhibits a definite charcoal appearance,
as opposed to the silvery appearance of 14-04-01. The exteriors are also different:
smooth versus foil-like. Note that the magnetic behavior of ingot 14-04-01 was stronger
than that of 14-04-02; yet both exhibited magnetic behavior not seen in natural aluminum.
See magnetic attraction section for a discussion of magnetic attraction in tailored
materials.
[0214] Similar differences in physical appearance were observed in manufactured copper ingots
as well. The observed physical differences between the two ingots were:
- 14-01-01 (Example 1 of USSN 10/123,028) had a void running approximately 1/3-1/2 the depth of the ingot; while 14-02-06
actually had major expulsion of material from the bath.
- 14-01-01 had the traditional copper color with some iridescence while the ingot 14-02-06
exhibited a strong red color, also with some iridescence and apparent band gap shift.
[0215] Interesting physical characteristics were also observable in copper ingots prepared
by one of the alternate techniques described herein. Based on alterations to the experimental
plan, for example changes to the third body addition and/or electromagnetic radiation
sources, the material outcome were significantly different.
[0216] Two copper ingots developed via an identical experimental plan except for the addition
of electromagnetic radiation through third-body addition. The surface of ingot 14-03-02
was smooth and exhibits what could be described as a "wood grain" finish. Ingot 14-03-03
exhibited a "dimpled" rough finish, with what appeared to be mosaic patterning. Material
expulsion to form a "crown" was also more significant in run 14-03-03. The color in
ingot 14-03-02 followed the traditional copper coloring more closely than 14-03-03
that exhibited a broader spectrum of colors including red and brown tones. As Table
2 shows, the induced elements were different for the two runs despite being prepared
in the same containment system, with identical operating conditions except for the
addition of EM radiation to third body gases. Hence, the composition of matter has
clearly been altered in both of these manufactured ingots.
Hardness Testing
[0217] Hardness testing was performed on material standards, natural copper, manufactured
copper prepared via the technique outlined in
U.S. Patent 6,572,792 B1, and manufactured copper prepared by the technique delineated herein. Two primary
hardness techniques were used: Rockwell Hardness and Moh's Hardness.
[0218] The Metals Handbook defines hardness as "Resistance of metal to plastic deformation,
usually by indentation." However, the term may also refer to stiffness or temper,
to resistance to scratching, abrasion, or cutting. Hardness testing does not give
a direct measurement of an engineering performance property; it correlates well with
strength, wear resistance, and other properties.
[0219] Rockwell Hardness testing is an indentation testing method in which an indenter is
impressed into the test sample at a prescribed load to measure the material's resistance
to deformation. A Rockwell hardness number is then calculated from the depth of permanent
deformation of the sample after application and removal of the test load. Various
indenter shapes and sizes combined with a range of test loads form a matrix of Rockwell
hardness scales.
[0220] Moh's Hardness testing is a scratch test in which known standards are used to scratch
materials to specify surface hardness through resistance to scratching. Interesting
test results were obtained in the testing of many of the manufactured ingots. For
example, a sample could exhibit an exceptionally high Moh's hardness (i.e., resistance
to scratching indicative of strong interfacial energy enhancement) yet shatter under
the Rockwell Hardness Test (i.e., highly brittle material).
[0221] A Moh's scratch test was performed on a manufactured Fe/V/Cr/Mn ingot. The surface
was impervious to scratching by the Moh's Standard for a hardness of 10, diamond.
In fact, the diamond tip was actually damaged by the manufactured alloy, indicating
that the tailored material had an apparent Moh's Hardness >10. Tool steel, a man-made
material of natural elements with a similar composition to this tailored ingot, typically
has a Moh's hardness between 6 and 7. This tailored material exhibited a hardness
far exceeding that which would be expected from natural materials and greater than
that which had been seen in any previous manufactured material (i.e., materials prepared
via the method presented in
U.S. Patent 6,572,792). Quite clearly, this process for tailoring material can significantly raise the
hardness, with an abundance of beneficial, commercially-relevant implications (e.g.,
drilling, mining, etc.).
[0222] Similar results on another tailored copper ingot compared with some standards provided
by the testing manufacturer. Note that the tailored material exhibited a very high
Moh's hardness factor and exhibited greater hardness in the radial direction than
in the axial direction. This anisotropic hardness behavior is generated through material
tailoring. Despite this Moh's hardness factor, the same tailored ingot exhibited brittle
failure during the Rockwell testing.
Magnetic and Material Attraction
[0223] Three different copper ingots were tailored via the techniques described herein.
Each of these ingots was subjected to a slightly different experimental protocol.
For example, the experimental program may have varied by the time, type, or method
of EM radiation addition. The resultant magnetic and physical attraction properties
of each ingot are significantly different from natural copper and significantly different
from each other. The attraction behavior of these three ingots is summarized in below:
Table 3: Attraction Behavior of Tailored Copper Ingots (9080 g, 99.98% purity)
Experimental Run Number |
Experimental Protocol/Method |
NdFeB Magnet Attraction |
Sulfur Attraction |
14-02-06 |
"HA" |
Observed |
Observed |
14-04-05 |
"HD" |
Observed |
Observed |
14-03-02 |
"AB" |
Observed |
Observed |
Natural Copper |
None |
None |
[0224] Each ingot exemplified magnetic attraction induced by the tailoring process: behavior
not present in natural copper. In addition to magnetic attraction, these ingots exhibited
attraction to other non-magnetic materials, such as sulfur. In each case, the testing
for the attraction behavior of the sulfur powder was performed on a clean, polished,
dry surface of the ingot to prohibit any effects of surface tension or adhesion. Additionally,
the areas of magnetic attraction and sulfur attraction were at significantly different
locations on the ingot, removing the possibility of induced attraction or other extraneous
surface effects.
[0225] Three important points to note:
- 1. The sulfur attraction was at different locations than the magnetic attraction,
eliminating induction, surface irregularities, surface adhesion, etc. as possible
explanations for the attraction.
- 2. The intensity of the sulfur attraction and the magnetic attraction mimicked each
other. That is, ingots that exhibit multiple points of magnetic attraction (widespread)
tend to have extensive regions of sulfur attraction.
- 3. The surfaces were polished, cleaned, and dried thoroughly before the testing was
performed. Analysis was performed in a fully vertical position.
[0226] Each of these points supports the supposition of a change in the composition of matter
affecting the electromagnetic behavior of the tailored material. Natural copper exhibits
no attraction to either magnets or sulfur. Yet, the manufactured copper, tailored
via three different protocols, all exhibited unique attraction behavior.
[0227] In addition to pure copper, various alloys were subjected to the experimental protocol
outlined herein and similar results were obtained: non-ferromagnetic material attraction,
ferromagnetic material attraction, and magnetic attraction.
[0228] The first example of such behavior is a Nickel/Rhenium ingot, Ingot 14-01-21. This
ingot, composed predominantly ofNi, will attract a magnet in its natural state. Hence,
no magnetic testing was performed. However the attraction of sulfur powder and various
ferromagnetic materials (Fe chips (99%
wt purity; 10-25 mesh), spherical sponge Fe (ranging from
-50 to
+100 mesh, 99.8%
wt pure), and Fe powder 94%
wt Fe, 3%
wt S, and 3%
wt C, none of which are attracted to natural nickel or rhenium in the absence of an
induced magnetic field caused by the presence of a magnet) were tested.
[0229] The Nickel/Rhenium tailored ingot exhibited unique material attraction throughout
the entire ingot (i.e., a volumetric property vs. a surface property) as exemplified
on multiple faces of the cut ingot. To further demonstrate that surface irregularities
are not the source of the unique attraction, an ingot was cut and the surface polished.
The clean, dry, polished surface was then used for evaluating the attraction behavior
of tailored materials.
[0230] In a similar emulation of the behavior observed in the tailored copper ingots, the
tailored Nickel/Rhenium ingot also exhibited significant attraction to sulfur powder.
[0231] To further demonstrate that the attraction behavior is caused by a change in the
composition of matter that in turn alters the electromagnetic behavior of the tailored
material, a polished surface of the Ni/Re tailored ingot was tested for sulfur attraction
(i.e., eliminate the effects of surface irregularities). Additionally, the ingot was
rotated 180°. The same attraction patterning was observed independent of vertical
orientation, eliminating a surface lip or defect as a possible explanation for the
attraction.
[0232] To demonstrate that the attraction behavior observed was not unique to nickel alloys
(e.g., due to their ferromagnetic behavior), a similar set of attraction experiments
was performed on a tailored copper ingot containing Cu, Re, Ag, and Au. Sulfur attraction
was achieved on multiple surfaces, in this instance, the top and the bottom.
[0233] This tailored copper alloy ingot exhibited multiple points of attraction to a Nd/Fe/B
magnet.
[0234] In yet another set of experiments to investigate the behavior of tailored ingots
that are ferromagnetic in their natural state (i.e., can be induced to have a magnetic
field, through the alignment of magnetic moments using a natural magnet), a tailored
cobalt alloy ingot (Co/V/Re Ingot 14-01-20) was tested for material attraction immediately
following the end of the tailoring process. The manufactured Co/V/Re ingot did attract
iron immediately following the tailoring process in limited regions.
[0235] Given these positive attraction-testing results, further tests were performed on
the tailored copper and copper alloy (non-ferromagnetic) ingots. These non-ferromagnetic
materials should not attract either a magnet or iron in their natural state. Yet,
each of the manufactured copper ingots attracted spherical sponge iron (99.8%
wt Pure,
-50 to
+100 mesh). Ingots 14-04-05, 14-04-03, 14-02-06, all exhibited a fairly random patterning
("sprinkling") of attraction, while ingot 14-03-02 appears to have definite "lines"
of attraction.
Magnetic Field Testing: Gauss Measurements
[0236] In a natural material, the attraction of a magnet or ferromagnet is accompanied by
the appearance of a magnetic field (caused by the alignment of magnetic moments in
the magnetic or ferromagnetic material creating a measurable field strength, magnetic
density or magnetic flux). Since each of these tailored materials exhibited an attraction
to a Nd/Fe/B magnet (and many attracted ferromagnetic iron), Gauss readings were taken
at designated intervals across the ingot surface to observe any potential magnetic
fields (using an F.W. Bell 4048 Gauss Meter). The detailed magnetic grids obtained
from such testing may be found in Appendix 3. The results are summarized in Table
4 below.
Table 4: Gauss Meter Readings Showing No Significant Measurable Magnetic Fields on
Tailored Ingots
Expt'I Run Number |
Tailored Material and Experimental "Method"/Protocol |
Significant Magnetic Field† |
Maximum Absolute Gauss Reading‡,†† |
14-04-05 |
Cu"HD" |
None |
0.0±0.2 |
14-02-06 |
Cu "HA" |
None |
0.0±0.2 |
14-03-02 |
Cu "AB" |
None |
0.0±0.2 |
14-01-21 |
Ni/Re "HD" |
None |
0.0±0.5 |
14-04-03 |
Cu/Re/Au/Ag "HD" |
None |
0.0±0.2 |
†The average magnetic field observed at the earth's surface is between 0.1-0.5 gauss. |
‡The maximum absolute gauss reading for natural, high purity (99.9%wt) copper was 0.0±0.2. |
††The maximum absolute gauss reading for natural, high purity (99.99%wt) nickel was 0.0±0.6. |
[0237] Note, no significant detectable magnetic field was observed on any of these tailored
ingots despite their ability to attract and hold a magnet at 90° (i.e., vertical orientation).
The measured gauss strengths are comparable to the background levels measured at the
earth's surface. The average magnetic field observed at the earth's surface is between
0.1-0.5 gauss. Commercially available magnets exhibit gauss strengths measured in
the 1000's: Nd/Fe/B magnets 10,500-14,000 gauss, SmCo 8,000-12,000 gauss, AlNiCo 6,000-13,500
gauss and Ferrite 2,000-4,000 gauss. In addition, the areas exhibiting the greatest
apparent magnetic force (0.5 gauss) were tested for attraction to iron filings. No
iron filings held on these particular locations.
[0238] The conclusions that can be drawn from this series of documented attractions:
• Tailored materials exhibit unique attraction to magnetic, ferromagnetic, and non-magnetic
materials that are not observed in natural materials.
• Unlike natural materials, tailored materials exhibit no correlation between observable
magnetic field strength (as measured by a gauss meter) and material attraction (magnetic,
ferromagnetic, or non-magnetic).
• The unique attraction properties of tailored materials are attributable to a change
in the electromagnetic behavior, indicative of a change in the composition of matter.
• These surface attractions are not attributable to surface irregularities or induced
magnetic fields as the tailored materials:
- 1. Have exhibited unique attraction in the "raw" and polished state, in multiple positions,
and on multiple surfaces (both internal and external).
- 2. Have attracted fine particles (sulfur and spherical iron sponge) and large particles
(1/8" diameter magnetic, iron chips).
- 3. Have exhibited multiple areas of attraction and those areas attracting sulfur are
not necessarily the same areas that attract ferromagnetic or magnetic materials. Similarly,
areas that attract magnets are not necessarily the areas that attract ferromagnets
or non-magnets.
[0239] Exhibit negligible magnetic field strengths as measured by an F.W. Bell 4048 gauss
meter.
1 Zee, A. Quantum Field Theory in a Nutshell. Princeton: Princeton U P, 2003
2 Wen, Xiao-Gang. Quantum Field Theory of Many-Body Systems. New York: Oxford U P, 2004
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Effect." Reviews of Modern Physics 71.2 (1999): S298-S305
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Princeton U P, 1997
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U P <http://www.msri.org/publications/books/gt3m>
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of Physics Publishing, 2003
7 Nash, Charles. Differential Topology and Quantum Field Theory. London: Academic P,
1991
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and Riemann Spaces of Kleinian Groups." Journal of the American Mathematical Society
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1 Keen, Linda and Caroline Series. "Pleating Coordinates for the Maskit Embedding of
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[0240] While this invention has been particularly shown and described with references to
preferred embodiments thereof, it will be understood by those skilled in the art that
various changes in form and details may be made therein without departing from the
scope of the invention encompassed by the appended claims.
[0241] The present application discloses:
- 1. A method of modifying the electronic structure of a material comprising the steps
of:
(1.) Melting the material;
(2.) Adding a carbon source to the material; and
(3.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein the material remains at a temperature above the melting point
during the entire step; and
(4) Cooling the material to room temperature; the improvement comprising at least
one of the following:
- (a) at least one gas is added to the material through a lance set at a level above
the liquid level;
- (b) at least one gas or gaseous additions comprises a gas mixture;
- (c) at least one gas or gaseous additions has been exposed to radiation;
- (d) current is added to the material in a further step or during one or more of the
above steps;
- (e) during the cooling step, a gas is added to the material;
- (f) during the cooling step, the material is quenched with water wherein the water
is not stirred;
- (g) at least one form of radiation has been filtered;
- (h) the material is exposed to radiation in a further step or during one or more of
the above steps; and/or
- (i) varying the reactor power between two power levels over 1/2, one or more cycles.
- 2. The method of paragraph 1 further comprising one or more of the steps, in one or
more iterations or cycles:
(5.) Adding a flow of a gas through the material;
(6.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein the material remains at a temperature above the melting point
during the entire step;
(7.) Adding a carbon source to the material; and/or
(8.) Holding the material with optional gas addition.
- 3. The method of paragraph 2 further comprising one or more of the steps, in one or
more iterations or cycles:
(9.) Lowering the temperature of a molten material, wherein the material becomes supersaturated
with carbon;
(10.) Varying the temperature of the material between two temperatures over one or
more cycles, wherein supersaturation with carbon is maintained and the material remains
at a temperature above the melting point during the entire step, optionally in the
presence of gas addition during the entire step or any portion of the step (e.g.,
during one or more or all of the steps wherein temperature increases or decreases);
(11.) Holding the material at a selected temperature, optionally in the presence of
gas addition; and/or
(12.) Cooling the material, such that the material continues to be supersaturated
with carbon and the material remains at a temperature above the melting point, optionally
in the presence of gas addition.
- 4. The method of paragraph 3 wherein steps 9, 10 and/or 11 are repeated at least one
time.
- 5. The method of paragraph 3 wherein steps 9, 10 and/or 11 are repeated at least four
times.
- 6. The method of paragraph 1 wherein the gas added to the material comprises a combination
of at least two of the following gases: hydrogen, helium, nitrogen, neon, argon, and
krypton.
- 7. The method of paragraph 1 wherein the gas has been exposed to radiation.
- 8. The method of paragraph 7 wherein the radiation is supplied by a short arc lamps,
high intensity discharge lamps, pencil lamps, lasers, light emitting diodes, incandescent,
fluorescent, infrared, ultraviolet, long wave ultraviolet and/or halogen.
- 9. The method of paragraph 7 wherein the radiation is supplied by a pencil lamp.
- 10. The method of paragraph 7 wherein the radiation is supplied by a high intensity
discharge lamp.
- 11. The method of paragraph 7 wherein the radiation is supplied by a short arc lamp.
- 12. The method of paragraph 7 wherein multiple radiation sources are used in combination.
- 13. The method of paragraph 1 wherein current is added to the material.
- 14. The method of paragraph 13 wherein the current is AC.
- 15. The method of paragraph 14 wherein the current is DC.
- 16. An apparatus comprising a combination of the following: (a) at least one pencil
lamp; (b) at least one high intensity discharge lamp within a housing; and (c) a material
produced by the method of paragraph 1.
- 17. The apparatus of paragraph 16 further comprising a light shield or a filter.
- 18. An apparatus comprising a combination of the following: (a) at least one pencil
lamp; (b) at least one short arc lamp within a housing; (c) a material produced by
the method of paragraph 1.
- 19. The apparatus of paragraph 18 further comprising a light shield or a filter.
- 20. An apparatus comprising (1) a reactor comprising an induction furnace characterized
by a first gas source and (2) at least one radiation source arranged to expose the
gas and/or the contents of the reactor.
- 21. The apparatus of paragraph 20 wherein the radiation source is one or more pencil
lamps.
- 22. The apparatus of paragraph 20 wherein the radiation source is one or more high
intensity discharge lamps.
- 23. The apparatus of paragraph 20 wherein the radiation source is one or more short
arc lamps.
- 24. The apparatus of paragraph 21 further comprising a light shield or a filter.
